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November
Summary
At about 1.25 am on the fourth of November 1975 the foreman at the Queen Victoria Blast Furnace, Appleby-Frodingham Works started a cast that was intended to fill two torpedo
Summary
At about 1.25 am on the fourth of November 1975 the foreman at the Queen Victoria Blast Furnace, Appleby-Frodingham Works started a cast that was intended to fill two torpedo ladles. Conditions at the time were normal; the shift manager was in attendance.
Shortly before 2.00 am some 175 tonnes of metal had been run into the first torpedo and the iron stream diverted to the second ladle. Some 10 to 15 minutes later the blow pipe at the No. 3 tuyere position started to burn down on the side facing on to No. 2 tuyere hearth cooler. The burning developed rapidly with intense flame and sparks despite efforts by the furnace keeper to cool the pipe by spraying it with water.
Whilst the pipe was burning down, a substantial water leak from the furnace or fittings was observed. The source of the leak could not be identified because the face of the furnace was obscured by flame. For the same reason men could not approach the leak to take remedial action. The leak of water was under pressure and fell outwards from the furnace towards the edge of the hob; from the hob the water ran down the slope of the cast house floor joining eventually with the iron runnel Water entered the full torpedo ladle.
Within a few minutes of the blow pipe starting to burn down progressive action was being taken by the furnace crew to bring the furnace off blast so that a new pipe could be fitted.
Shortly before 2.47 am instructions from the shift manager were passed via Traffic Control to a loco driver and shunter to remove the full torpedo ladle from the vicinity of the furnace. Traffic personnel were made aware that water was running into the torpedo. As the loco was coupled to the ladle, water was seen to be coming from the iron runner. An explosion occurred as the ladle was moved. An eye witness identified the throat of the ladle as the seat of the explosion. The incident was timed at 2.47 am.
As a result of the explosion there were four immediate fatalities and 15 hospital admissions. Subsequently a further seven employees died as a result of injuries received.
At the time of the explosion 23 persons were working in the Queen Victoria furnace area. This number included four extra helpers standing by to assist in changing No. 3 blast pipe. Casting to the second torpedo was sti11 proceeding at the time of the explosion.
Report: https://www.icheme.org/media/13691/the-explosion-at-appleby-frodingham-steelworks-scunthorpe.pdf
Image Credit: HSE
Summary
The Valero Delaware City refinery asphyxiation death of two contractor employees who were preparing to reassemble a pipe on a pressure vessel while it was being purged with nitrogen. The
Summary
The Valero Delaware City refinery asphyxiation death of two contractor employees who were preparing to reassemble a pipe on a pressure vessel while it was being purged with nitrogen. The first worker, in an attempt to retrieve a roll of tape from inside the vessel, was overcome by nitrogen, collapsed in the vessel, and died. His co-worker, the crew foreman, was asphyxiated while attempting to rescue him.
KEY ISSUES:
• OXYGEN-DEFICIENT ATMOSPHERE HAZARDS OUTSIDE CONFINED SPACE OPENINGS
• NITROGEN HAZARD AWARENESS
• UNPLANNED CONFINED SPACE RESCUE
ROOT CAUSES:
1. Workers suddenly involved in emergency activities allow emotions to override safe work procedures and training.
Image credit: CSB

Related Events
Summary
An explosion in a chemical facility. A gas cloud was seen above the area immediately after the explosion. Damaged about 20 buildings and left a crater in the facility’s backyard Proximate
Summary
An explosion in a chemical facility. A gas cloud was seen above the area immediately after the explosion. Damaged about 20 buildings and left a crater in the facility’s backyard
Proximate causes:
• Inadequate tools, equipment & vehicles
• Inadequate engineering/design
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: Unidentified
Summary
Early on 7 November 1975, start-up of the Naphtha cracker commenced on the ethylene plant at the Dutch State Mines (DSM) works at Beek. At 06:00 hours compressed gas was
Summary
Early on 7 November 1975, start-up of the Naphtha cracker commenced on the ethylene plant at the Dutch State Mines (DSM) works at Beek. At 06:00 hours compressed gas was sent to the low temperature system. At 09:48 hours an escape of vapour occurred from the depropaniser which ignited, resulting in a massive vapour cloud explosion. The explosion caused significant damage and started numerous fires around the plant. 14 people were killed and a total of 107 people injured, three of whom were outside of the site.
The investigation was hampered by the destruction of instrument records in the incident but evidence suggested that the release was due to low temperature embrittlement at the depropaniser feed drum. It was thought that the initial fracture had occurred on a 40 mm pipe connecting the feed drum to its relief valve. The normal operating temperature of the drum was 65°C, however, due to a process upset in the de-ethaniser column, the stream feeding into the depropaniser drum was a liquid at about 0°C(or lower) with a high C2 content. This would flash within the drum resulting in a temperature which could be as low as -10°C. The feed drum material could normally be used at temperatures as low as -20°C, however the fracture occurred at a weld, which with ageing may fail at up to 0°C.
The raising of the alarm was also flawed. The first operator to enter the control room to report the gas release was distressed and shocked. A second operator left the room to investigate, leaving orders for the fire alarm to be sounded. This did not occur. Some witnesses stated that the alarm system failed, but the investigation found that the system was in good working order before the explosion, and that none of the button switches had been operated.
KEY ISSUES:
• DESIGN CODES – PLANT
• EMERGENCY RESPONSE / SPILL CONTROL
Image Credit: Nationaal Archief
Summary
At the premises of Corus UK Ltd, Port Talbot, No. 5 Blast Furnace exploded at approximately 17.13 pm on 8 November 2001. The entire furnace, which with its contents weighed
Summary
At the premises of Corus UK Ltd, Port Talbot, No. 5 Blast Furnace exploded at approximately 17.13 pm on 8 November 2001. The entire furnace, which with its contents weighed approximately 5000 tonnes, lifted bodily at the lap joint, rising some 0.75 m from its supporting structures, leading to the explosive release of hot materials (an estimated 200 tonnes in total, comprising largely solids and semisolids, with a little molten metal) and gases into the cast house.
Three employees died: Andrew Hutin, Stephen Galsworthy and Len Radford. A further 12 employees and contractors sustained severe injuries. Many more suffered minor injuries and shock.
Report: https://www.icheme.org/media/10689/the-explosion-of-no-5-blast-furnace-corus-uk-ltd-port-talbot.pdf
Image Credit: HSE
Summary
November 9, 2010 explosion at an E.I. duPont de Nemours and Co. Inc., Yerkes chemical plant in Buffalo, New York when a contract welder and foreman were repairing the agitator
Summary
November 9, 2010 explosion at an E.I. duPont de Nemours and Co. Inc., Yerkes chemical plant in Buffalo, New York when a contract welder and foreman were repairing the agitator support atop an atmospheric storage tank containing flammable vinyl fluoride. The welder died instantly from blunt force trauma, and the foreman received first-degree burns and minor injuries. The explosion blew most of the top off the tank. The top and agitator assembly hung over the side of the tank supported only by a 2-foot section of the top (cover photo). The explosion caused minor overpressure damage in the tank farm area and the adjacent production building.
KEY ISSUES:
• FLAMMABLE GAS MONITORING
• TANK ISOLATION
• HOT WORK PERMITS, PROCEDURES & SIGN-OFFS
ROOT CAUSES:
1. All potential explosion hazards associated with hot work activities not identified and mitigated
2. All relevant forms required for permits not completed in accordance with corporate policies and industry standards (including NFPA 326 and NFPA 51B)
3. Appropriate DuPont personnel did not officially approve hot work permits, by signature or equivalent, consistent with DuPont policies
Image credit: CSB

Related Events
Summary
An explosion occurred in an air line in a reactor used for the liquid phase oxidation of butane as it was being started up. The explosion ruptured the external portion
Summary
An explosion occurred in an air line in a reactor used for the liquid phase oxidation of butane as it was being started up. The explosion ruptured the external portion of the air line to the reactor, allowing the reactor contents to vaporize and form a cloud. The vapor cloud drifted and ignited about 25 to 30 seconds after the initial release. There was extensive property damage in the immediate area as a result of the vapor cloud explosion and significant damage throughout the site. Windows were broken seven miles away. The immediate cause was believed to be insufficient purging of the reactor when it had previously been down.
[ Property Damage $215 Million. Estimated Current Value $516 Million ]
Image credit: The Center For Land Use Interpretation
Summary
On November 15, 2014, approximately 24,000 pounds of highly toxic methyl mercaptan was released from an insecticide production unit (Lannate® Unit) at the E. I. du Pont de Nemours and
Summary
On November 15, 2014, approximately 24,000 pounds of highly toxic methyl mercaptan was released from an insecticide production unit (Lannate® Unit) at the E. I. du Pont de Nemours and Company (DuPont) chemical manufacturing facility in La Porte, Texas. The release killed three operators and a shift supervisor inside a manufacturing building. They died from a combination of asphyxia and acute exposure (by inhalation) to methyl mercaptan.
KEY ISSUES:
• EMERGENCY PLANNING & RESPONSE (PREPAREDNESS)
• IMPLEMENTATION OF PROCESS SAFETY MANAGEMENT SYSTEMS
• ASSESSMENT OF PROCESS SAFETY CULTURE
ROOT CAUSES:
1. DuPont’s corporate process safety management system did not ensure that DuPont La Porte implemented and maintained an effective process safety management system; and
2. DuPont La Porte did not assess its culture for process safety in the site’s Safety Perception Surveys or any other formal assessment program, allowing serious process safety deficiencies to exist at the site.
Image credit: CSB

Summary
A gas explosion that occurred inside a coal mine in northern China has claimed the lives of 15 miners and left another nine injured, according to authorities. The blast took
Summary
A gas explosion that occurred inside a coal mine in northern China has claimed the lives of 15 miners and left another nine injured, according to authorities. The blast took place at a mine operated by the Feng Yan Group in Pingyao County, Shanxi province.
Following the explosion, 11 miners managed to escape without injury.
The mine, which is proportionally small, was in the news last year due to its failure in providing adequate training for workers. Xinhua quoted the Shanxi Administration of Coal Mine Safety as saying that 35 miners were working underground at that time.
Shanxi Administration of Coal Mine Safety accident investigation division director Shen Xuping said: “It is a production safety accident caused by production activity that broke the law and regulations, which reveals the problems of the involved company, such as lack of awareness of the rule of law and chaotic management.”
Authorities are currently carrying out an investigation to determine the cause of the explosion.
Image Credit: AFP / Getty
Summary
On Friday 19 November 2010 at 3:45pm there was an underground explosion at the Pike River coal mine. Twenty-nine men lost their lives, and their bodies have not been recovered. Two
Summary
On Friday 19 November 2010 at 3:45pm there was an underground explosion at the Pike River coal mine. Twenty-nine men lost their lives, and their bodies have not been recovered.
Two men survived the explosion. They were in the stone access tunnel (drift), a distance from the pit bottom area where the main workplaces were located. Although initially overcome, Daniel Rockhouse rescued himself and his colleague Russell Smith.
The New Zealand Police led the emergency response that involved emergency services, and mines rescue crews from New Zealand, New South Wales and Queensland. Despite strenuous efforts by everyone involved, a lack of information concerning the conditions underground prevented a rescue attempt.
A second explosion on Wednesday 24 November extinguished any hope of the mens survival. The emergency focus changed to recovery of the bodies.
Image Credit: AFP
Summary
Following torrential rain, rising floodwater allowed waste oil floating on the surface to be brought into contact with hot equipment on the refinery causing explosions and a fire. A second
Summary
Following torrential rain, rising floodwater allowed waste oil floating on the surface to be brought into contact with hot equipment on the refinery causing explosions and a fire. A second blaze broke out and several storage tanks reportedly caught fire and exploded. Damage to the refinery was extensive, two were killed, and a further three reported missing. Later reports said that two to three production units had been affected by the fire. The processing units affected were the crude unit, the 20,000 bbl-per-day vacuum distillation unit, the 24,000 bbl-per-day catalytic reformer unit, and the 24,000 bbl-per-day distillate hydrotreater. At the time, it was stated that the units not affected by the fire would restart within 15 days, although the other units would not be operational for a further eight to 12 months.
[ Property Damage $130 Million. Estimated Current Value $213 Million ]
Image credit: Samir
December
Summary
An explosion ripped through the New Cumberland A.L. Solutions titanium plant in West Virginia on December 9, 2010, fatally injuring three workers. The workers were processing titanium powder, which is
Summary
An explosion ripped through the New Cumberland A.L. Solutions titanium plant in West Virginia on December 9, 2010, fatally injuring three workers. The workers were processing titanium powder, which is highly flammable, at the time of the explosion.
KEY ISSUES:
• FEDERAL COMBUSTIBLE DUST OVERSIGHT
• HAZARD RECOGNITION & TRAINING
• LEARNING FROM PREVIOUS INCIDENTS
ROOT CAUSES:
1. AL Solutions did not mitigate the hazards of metal dust explosions through engineering controls, such as a dust collection system. Specifically, AL Solutions did not adhere to the practices recommended in NFPA 484 for controlling combustible metal dust hazards.
Image credit: CSB

Related Events
Summary
An explosion occurred in the ammonium nitrate process area of this plant. As a result of the explosion, the seven-story main process building was completely destroyed and a 30-foot-diameter crater
Summary
An explosion occurred in the ammonium nitrate process area of this plant. As a result of the explosion, the seven-story main process building was completely destroyed and a 30-foot-diameter crater was created. Metal fragments from the explosion punctured one of the plant’s two 15,000-metric-ton refrigerated ammonia storage tanks. The punctured tank released an estimated 5,700 metric tons of ammonia, causing the evacuation of approximately 2,500 people from the surrounding area. Metal fragments also punctured a nitric acid tank, resulting in the release of approximately 100 metric tons of this acid. The explosion tore metal siding from adjacent buildings, damaged three third-party electric generating stations, broke windows of buildings 16 miles away in Sioux City, and was felt more than 30 miles away.
[ Property Damage $203 Million. Estimated Current Value $404 Million ]
Image credit: EPA
Ref: https://en.wikipedia.org/wiki/Port_Neal_fertilizer_plant_explosion
Summary
At 1:33 pm on December 19, 2007, a powerful explosion and subsequent chemical fire killed four employees and destroyed T2 Laboratories, Inc. (T2), a chemical manufacturer in Jacksonville, Florida. It
Summary
At 1:33 pm on December 19, 2007, a powerful explosion and subsequent chemical fire killed four employees and destroyed T2 Laboratories, Inc. (T2), a chemical manufacturer in Jacksonville, Florida. It injured 32, including four employees and 28 members of the public who were working in surrounding businesses. Debris from the reactor was found up to one mile away, and the explosion damaged buildings within one quarter mile of the facility.
On December 19, T2 was producing its 175th batch of methylcyclopentadienyl manganese tricarbonyl (MCMT). At 1:23 pm, the process operator had an outside operator call the owners to report a cooling problem and request they return to the site. Upon their return, one of the two owners went to the control room to assist. A few minutes later, at 1:33 pm, the reactor burst and its contents exploded, killing the owner and process operator who were in the control room and two outside operators who were exiting the reactor area.
KEY ISSUES:
• REACTIVE HAZARD RECOGNITION
• HAZARD EDUCATION
• EMERGENCY PREPAREDNESS
• PROCESS DESIGN & SCALE-UP
ROOT CAUSES:
• T2 did not recognize the runaway reaction hazard associated with the MCMT it was producing.
Image credit: CSB

Summary
An eight-inch-diameter pipeline operating at approximately 700-pounds-per-square-inch ruptured, releasing a mix of ethane and propane. The record low temperature of 10°F for the region is believed to have contributed to
Summary
An eight-inch-diameter pipeline operating at approximately 700-pounds-per-square-inch ruptured, releasing a mix of ethane and propane. The record low temperature of 10°F for the region is believed to have contributed to the rupture. After a few minutes, the resulting release was ignited, causing a vapor cloud explosion. The explosion shattered windows up to six miles away and could be felt as far as 15 miles away. Seventeen additional pipelines, in a pipe rack containing 70 lines, were ruptured by the explosion.
The resulting fire involved two large storage tanks holding 3.6 million gallons of diesel, 12 small tanks containing a total of 882,000 gallons of lube oil, and two separator units. The explosion resulted in the partial loss of electricity, steam, and fire water for the refinery, since two power lines, two steam lines and a 12-inch diameter fire water line were located in this pipe rack. Upon the initial explosion, the lines for the dock fire pumps were damaged. Therefore, the water for fire fighting had to be supplied with the remaining plant fire pumps and municipal fire trucks taking draught from alternate sources. Approximately 48,000 gallons of aqueous film-forming foam (AFFF) concentrate, 200 fire brigade members, and 13 pumper units were used during the fire fighting effort, which was successful in extinguishing the fire approximately 14 hours after the initial explosion. Because of this incident, the refinery was completely shut down for three days and operated at reduced capacity for an additional three weeks.
[ Property Damage $69 Million. Estimated Current Value $155 Million ]
Image credit: Sam Kittner
January
Summary
On 4th January 1966, an operation to drain off an aqueous layer from a propane storage sphere was attempted. Two valves were opened in series on the bottom of the
Summary
On 4th January 1966, an operation to drain off an aqueous layer from a propane storage sphere was attempted. Two valves were opened in series on the bottom of the sphere. When the operation was nearly complete, the upper valve was closed and then cracked open again. No flow came out of the cracked valve, so it was opened further. The blockage, assumed to be ice or hydrate, cleared and propane gushed out. The operator was unable to close the upper valve and by the time he attempted to close the lower valve this was also frozen open. The alarm was raised and traffic on the nearby motorway was stopped. The resulting vapour cloud is thought to have found its source of ignition from a car about 160 m away. The storage sphere was enveloped in a fierce fire and upon lifting of the relief valve a stream of escaping vapour was ignited.
The LPG tank farm where the sphere was located consisted of four 1200 m3 propane and four 2000 m3 butane spheres. The fire brigade arrived on site, but were not experienced in dealing in refinery fires, and it appears they did not attempt to cool the burning sphere. They concentrated their hoses on cooling the remaining spheres. About 90 minutes after the initial leakage, the sphere ruptured, killing the men nearby. A wave of liquid propane flowed over the compound wall and fragments of the ruptured sphere cut through the legs of the next sphere which toppled over. The relief valve on this tank began to emit liquid.
The fire killed 18 people and injured 81 others. Five of the storage spheres were destroyed.
KEY ISSUES:
• DESIGN CODES – PIPEWORK
• SECONDARY CONTAINMENT
• OPERATING PROCEDURES
• EMERGENCY RESPONSE / SPILL CONTROL
• DESIGN CODES – PLANT
Image Credit: Fonds Georges Vermard
Related Events
Lessons
IChemE S&LP: Feyzin Incident Summary (04-Jan-66) (icheme.org)
Summary
One worker died after hazardous chemical vapors released from an over-pressurized reactor burned his respiratory system. The worker charged chemicals inside a reactor vessel and a reaction started before he
Summary
One worker died after hazardous chemical vapors released from an over-pressurized reactor burned his respiratory system. The worker charged chemicals inside a reactor vessel and a reaction started before he could close it.
OSHA’s proposed penalties total $87,780
Proximate causes:
• Inadequate management/supervision
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: Google Maps
Summary
On January 7, 1998, two explosions in rapid succession destroyed the Sierra Chemical Company Kean Canyon plant near Mustang, Nevada, killing four workers and injuring six others. The Kean Canyon plant
Summary
On January 7, 1998, two explosions in rapid succession destroyed the Sierra Chemical Company Kean Canyon plant near Mustang, Nevada, killing four workers and injuring six others.
The Kean Canyon plant manufactured explosive boosters for the mining industry. When initiated by a blasting cap or detonation cord, boosters provide the added energy necessary to detonate less sensitive blasting agents or other high explosives. The boosters manufactured at the Kean Canyon plant consisted of a base mix and a second explosive mix, called Pentolite, both of which were poured into cardboard cylinders. The primary explosives used in the base mix were TNT (2,4,6-trinitrotoluene), PETN (pentaerythritol tetranitrate), and Comp-B, a mixture of TNT and RDX (hexahydro-1,3,5-trinitro-1,3,5-triazine). The Pentolite is a mix of TNT and PETN.
KEY ISSUES:
• PROCESS SAFETY MANAGEMENT
• WORKER TRAINING
• PROCESS HAZARD ANALYSIS
• LANGUAGE BARRIERS
ROOT CAUSES:
1. Process hazard analysis (PHA) conducted by the facility was inadequate.
2. Training programs for facility personnel were inadequate.
3. Written operating procedures were inadequate or not available to workers.
4. The facility was built with insufficient separation distances between different operations and the design and construction of buildings was inadequate.
5. There was no systematic safety inspection or auditing program.
6. The employee participation program was inadequate.
Image Credit: CSB

Summary
An 11-year-old, 121,000-deadweight-ton tanker had completed unloading its first parcel of Arabian heavy crude when a small fire was noticed on deck. About 10 minutes later, fire spread to both
Summary
An 11-year-old, 121,000-deadweight-ton tanker had completed unloading its first parcel of Arabian heavy crude when a small fire was noticed on deck. About 10 minutes later, fire spread to both sides of the ship. Later, a massive explosion occurred. The initiating event of the disaster was likely the buckling of the ship’s structure at deck level. Explosions in the ballast tanks and the breaking of the ship’s back followed. These events were produced by the conjunction of two separate factors: a seriously weakened hull due to inadequate maintenance and an excessive stress due to incorrect ballasting at the time of the disaster. In addition to the total loss of the ship, 1,130 feet of the concrete and steel jetty were damaged or destroyed.
[ Property Damage $70 Million. Estimated Current Value $248 Million ]
Image credit: Irish Times
Summary
On Wednesday, January 11, 2006, three workers continued the roof removal. About 11:15 a.m., the lead mechanic and the third worker were cutting the metal roof directly above the methanol
Summary
On Wednesday, January 11, 2006, three workers continued the roof removal. About 11:15 a.m., the lead mechanic and the third worker were cutting the metal roof directly above the methanol tank vent. Sparks, showering down from the cutting torch, ignited methanol vapors coming from the vent, creating a fireball on top of the tank. The fire flashed through a flame arrester on the vent, igniting methanol vapors and air inside the tank, causing a explosion inside the steel tank.
The explosion inside the methanol storage tank
• rounded the tank’s flat bottom, permanently deforming the tank and raising the side wall about onefoot;
• ripped the nuts from six bolts used to anchor the tank to a concrete foundation;
• blew the flame arrester off the tank vent pipe;
• blew a level sensor off a 4-inch flange on the tank top;
• separated two 1-inch pipes, valves, and an attached level switch from flanges on the side of the tank;
• separated a 4-inch tank outlet pipe from the tank outlet valve; and
• separated a 4-inch tank fill pipe near the top the tank.
Methanol discharged from the separated pipes ignited and burned, spreading the fire. Methanol also flowed into the containment around the tank and through a drain to the WWTP where it was diluted and harmlessly processed. The lead mechanic and the third worker were in the man-lift basket over the methanol tank when the ignition occurred. They were likely burned from the initial fireball and burning methanol vapors discharging from the tank vent under pressure from the explosion. The lead mechanic, fully engulfed in fire, likely jumped or fell from the man-lift. Emergency responders found his body within the concrete containment next to the tank.
The third worker stated that he had been partially out of the man-lift basket leaning over the roof when the fire ignited. On fire, he climbed onto the roof to escape. Co-workers, unable to reach him with a ladder, told him to jump to an adjacent lower roof and then to the ground. He sustained second and third degree burns over most of his body, and was hospitalized for 4 months before being released to a medical rehabilitation facility. Methanol sprayed from separated pipes onto the crane, burning the crane cab with the mechanic inside. On fire, he exited the cab and was assisted by co-workers. He died in the hospital the following day.
KEY ISSUES:
• HAZARD COMMUNICATION
• HOT WORK CONTROL
• PLASTIC PIPE IN FLAMMABLE SERVICE
• FLAME ARRESTER MAINTENANCE
• FLORIDA PUBLIC EMPLOYEE SAFETY PROGRAMS
ROOT CAUSES:
1. The City of Daytona Beach did not implement adequate controls for hot work at the Bethune Point WWTP.
2. The City of Daytona Beach had a hazard communication program that did not effectively communicate the hazards associated with methanol at the Bethune Point WWTP.
Image credit: CSB

Summary
On January 13, 2003, at approximately 4:30 pm, a vapor cloud deflagration and pool fire erupted at the BLSR Operating, Ltd. (BLSR), facility located 5 miles north of Rosharon, Texas.
Summary
On January 13, 2003, at approximately 4:30 pm, a vapor cloud deflagration and pool fire erupted at the BLSR Operating, Ltd. (BLSR), facility located 5 miles north of Rosharon, Texas. Two BLSR employees were killed, and three were seriously burned. Two T&L Environmental Services, Inc. (T&L), truck drivers, who had just delivered gas condensate storage tank basic sediment and water (BS&W) to BLSR, were seriously burned; one of these men died on March 2.
The fire was caused by the release of hydrocarbon vapor during the unloading of BS&W from two vacuum trucks into an open area collection pit. BS&W is an oil/gas exploration and production (E&P) waste liquid. The fire destroyed two 50-barrel (2,100-gallon) vacuum trucks and seriously damaged waste liquid offloading equipment and structures at BLSR. One of the vacuum truck diesel engines was the most likely source of ignition..
KEY ISSUES:
• RECOGNIZING FLAMMABILITY HAZARDS OF EXPLORATION & PRODUCTION WASTE LIQUIDS
• SAFE HANDLING OF FLAMMABLE LIQUIDS
ROOT CAUSES:
1. Noble Energy, Inc., the shipper, failed to identify the flammability hazard of BS&W generated at its gas well production facility, and also failed to communicate the hazard to employees and contractors who were required to handle the flammable liquid.
2. T&L management did not require Noble Energy to provide vacuum truck drivers with a material safety data sheet or other document listing the potential flammability hazard of BS&W, nor did it identify the flammability hazard of the mixture in the vacuum truck tank.
3. BLSR management did not have effective hazard communication practices in place to recognize the potential flammability hazard of each shipment of BS&W, nor did it implement safe handling practices when offloading flammable liquid onto the mud disposal and washout pad area.
Image Credit: CSB

Summary
On January 16, 2002, highly toxic hydrogen sulfide gas leaked from a sewer manway at the Georgia-Pacific Naheola mill in Pennington, Alabama. Several people working near the manway were exposed
Summary
On January 16, 2002, highly toxic hydrogen sulfide gas leaked from a sewer manway at the Georgia-Pacific Naheola mill in Pennington, Alabama. Several people working near the manway were exposed to the gas. Two contractors from Burkes Construction, Inc., were killed. Eight people were injured–seven employees of Burkes Construction and one employee of Davison Transport, Inc. Choctaw County paramedics who transported the victims to hospitals reported symptoms of hydrogen sulfide exposure.
KEY ISSUES:
• REACTIVE HAZARD IDENTIFICATION
• HYDROGEN SULFIDE SAFETY
• EMERGENCY RESPONSE
ROOT CAUSES:
1. Good engineering and process safety practices were not followed when joining the drain from the truck unloading station and the oil pit to the acid sewer.
2. There was no management system to incorporate hazard warnings about mixing sodium hydrosulfide (NaSH) with acid into process safety information.
Image Credit: CSB

Summary
An explosion at a liquefied natural gas (LNG) plant resulted in 27 people killed, 72 injured, and seven reported missing. The explosion destroyed three out of six liquefaction trains, damaged
Summary
An explosion at a liquefied natural gas (LNG) plant resulted in 27 people killed, 72 injured, and seven reported missing. The explosion destroyed three out of six liquefaction trains, damaged a nearby power plant, and led to the shutdown of a 335,000 bbl per day refinery. There was also some damage to the neighboring industrial facilities. A faulty boiler was initially blamed for the incident. Investigations, however, indicated that a large release of hydrocarbon from a cold-box exchanger was ignited upon ingestion into the boiler. Train six of the LNG complex re-started in May 2004 and trains five and 10 in September 2004. Trains 20, 30, and 40 were destroyed in the incident, representing 50% of the capacity of the LNG complex.
[ Property Damage $470 Million. Estimated Current Value $689 Million ]
Image credit: Sonatrach
Summary
The incident occurred when workers were weighing a barrel of 4-hydroxybenzohydrazide. There was a short circuiting in the weighing scale which led to an explosion. Proximate causes: • Defective equipment Source:
Summary
The incident occurred when workers were weighing a barrel of 4-hydroxybenzohydrazide. There was a short circuiting in the weighing scale which led to an explosion.
Proximate causes:
• Defective equipment
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: Survival Technologies
Summary
On January 21, 1997, an explosion and fire occurred at the Hydrocracker Unit of the Tosco Refinery at Martinez, California, resulting in one death, 46 worker injuries and precautionary sheltering-in-place
Summary
On January 21, 1997, an explosion and fire occurred at the Hydrocracker Unit of the Tosco Refinery at Martinez, California, resulting in one death, 46 worker injuries and precautionary sheltering-in-place for the surrounding community. The accident involved the release and autoignition of a mixture of flammable hydrocarbons and hydrogen under high temperature and pressure. EPA undertook an investigation into the causes and underlying circumstances associated with this accident because of its serious consequences (fatality, injuries and offsite concern), the potential for greater impacts, and the opportunity to learn from this accident how similar accidents could be prevented
Image Credit: EPA
Summary
On January 22, 2018, a blowout and rig fire occurred at Pryor Trust 0718 gas well number 1H-9, located in Pittsburg County, Oklahoma. The fire killed five workers, who were
Summary
On January 22, 2018, a blowout and rig fire occurred at Pryor Trust 0718 gas well number 1H-9, located in Pittsburg County, Oklahoma. The fire killed five workers, who were inside the driller’s cabin on the rig floor. They died from thermal burn injuries and smoke and soot inhalation. The blowout occurred about three-and-a-half hours after removing drill pipe (‘tripping’) out of the well.
The cause of the blowout and rig fire was the failure of both the primary barrier (hydrostatic pressure produced by drilling mud) and the secondary barrier (human detection of influx and activation of the blowout preventer) which were intended to be in place to prevent a blowout.
KEY ISSUES:
• POOR BARRIER MANAGEMENT
• UNDERBALANCED OPERATIONS PERFORMED WITHOUT PROPER PLANNING, PROCEDURES, OR NEEDED EQUIPMENT
• SIGNS OF INFLUX EITHER NOT IDENTIFIED OR INADEQUATELY RESPONDED TO
• ALARM SYSTEM OFF
• FLOW CHECKS NOT CONDUCTED
• GAPS IN SAFETY MANAGEMENT SYSTEM
• DRILLER’S CABIN DESIGN
• BOP COULD NOT CLOSE DUE TO BURNED HYDRAULIC HOSES
• LACK OF SAFETY REQUIREMENTS BY REGULATION
ROOT CAUSES:
1. Failure of primary barrier – hydrostatic pressure produced by drilling mud.
2. Failure of secondary barrier – human detection of influx and activation of the blowout preventer.
Image & AcciMap Credit: CSB
Image credit: CSB

Summary
On January 22 and 23, 2010, three separate incidents at the DuPont plant in Belle, WV, involving releases of methyl chloride, oleum, and phosgene, triggered notification of outside emergency response
Summary
On January 22 and 23, 2010, three separate incidents at the DuPont plant in Belle, WV, involving releases of methyl chloride, oleum, and phosgene, triggered notification of outside emergency response agencies. The incident involving the release of phosgene gas led to the fatal exposure of a worker performing routine duties in an area where phosgene cylinders were stored and used.
Operators discovered the first incident, the release of methyl chloride, the morning of January 22, 2010, when an alarm sounded on the plant’s distributed control system monitor. They confirmed that a release had occurred and that methyl chloride was venting to the atmosphere. Managers assessing the release estimated that more than 2,000 pounds of methyl chloride may have been released over the preceding 5 days.
The oleum release, the second incident, occurred the morning of January 23, 2010. Workers discovered a leak in an overhead oleum sample pipe that was allowing a fuming cloud of oleum to escape to the atmosphere. The plant fire brigade, after donning the appropriate personal protective equipment, closed a valve that stopped the leak about an hour after it was discovered. No injuries occurred, but the plant called the Belle Volunteer Fire Department to assist.
The third incident, a phosgene release, occurred later that same day when a hose used to transfer phosgene from a 1-ton cylinder to a process catastrophically failed and sprayed a worker in the face while he was checking the weight of the cylinder. The employee, who was alone when exposed, was assisted by co-workers who immediately responded to his call for help. Initial assessments by the plant’s occupational health nurse indicated that the worker showed no symptoms of exposure prior to transport to the hospital for observation and treatment. A delayed onset of symptoms, consistent with information in phosgene exposure literature, occurred after he arrived at the hospital. His condition deteriorated over the next day and he died from his exposure the next night.
KEY ISSUES:
• MECHANICAL INTEGRITY
• ALARM MANAGEMENT
• OPERATING PROCEDURES
• COMPANY EMERGENCY RESPONSE & NOTIFICATION
ROOT CAUSES:
Methyl Chloride Incident (January 22, 2010)
1. DuPont management, following their Management of Change process, approved a design for the rupture disc alarm system that lacked sufficient reliability to advise operators of a flammable methyl chloride release.
Oleum Release Incident (January 23, 2010)
1. Corrosion under the insulation caused a small leak in the oleum pipe.
Phosgene Incident (January 23, 2010)
1. DuPont’s phosgene hazard awareness program was deficient in ensuring that operating personnel were aware of the hazards associated with trapped liquid phosgene in transfer hoses.
2. DuPont relied on a maintenance software program that was subject to changes without authorization or review, did not automatically initiate a change-out of phosgene hoses at the prescribed interval, and did not provide a back-up process to ensure timely change-out of hoses.
3. DuPont Belle’s near-miss reporting process was not rigorous enough to ensure that the near failure of a similar phosgene transfer hose, just hours prior to the exposure incident, would be immediately brought to the attention of plant supervisors and managers.
4. DuPont lacked a dedicated radio/telephone system and emergency notification process to convey the nature of an emergency at the Belle plant, thereby restricting the ability of personnel to provide timely and quality information to emergency responders.
Image credit: CSB

Summary
The massive explosion fatally injured two workers and caused extensive damage to nearby structures. Image credit: CSB
Summary
The massive explosion fatally injured two workers and caused extensive damage to nearby structures.
Image credit: CSB

Summary
During the early morning hours of January 25, ASCO employees filled cylinders with purchased acetylene. At approximately 9:30 am, with the depletion of the supply of purchased acetylene, they began
Summary
During the early morning hours of January 25, ASCO employees filled cylinders with purchased acetylene. At approximately 9:30 am, with the depletion of the supply of purchased acetylene, they began to produce acetylene from calcium carbide in the generator.
Because of heavy snowfall, workers were shoveling snow in the area south of the decant tanks near the loading dock. At 10:36 am, an explosion occurred, centered in the shed. Two of the workers immediately south of the shed were killed instantly. A third worker farther south, closer to the loading dock, was severely injured and was pronounced dead shortly after arriving at the Newark Medical Center. A fourth worker who was in the loading dock/lime pit area was very seriously injured by the blast. .
KEY ISSUES:
• OPERATING PROCEDURES
• STAFF TRAINING
• DRAIN & VENT TO SAFE LOCATION
• BUILDINGS TO BE DESIGNED FOR ACETYLENE CONTAINMENT
• MECHANICAL INTEGRITY
• POSITIVE ISOLATION
ROOT CAUSES:
1. At ASCO, a line that could potentially contain acetylene drained into an enclosed wooden shed.
2. The shed in this incident was not designed or constructed in accordance with NFPA 51A.
3. At ASCO the check valve was relied upon to prevent backflow. The check valve and block valve that failed at ASCO and allowed backflow were not on a testing or inspection schedule. The single block valve on the recycle water line, which was found closed after the explosion, leaked during post-incident testing.
4. Operators did not use either written operating procedures or check lists for start up of the acetylene generator or recycled water system at this facility.
Image Credit: CSB

Related Events
Summary
The Space Shuttle Challenger disaster was a fatal incident in the United States space program that occurred on Tuesday, January 28, 1986, when the Space Shuttle Challenger (OV-099) broke apart
Summary
The Space Shuttle Challenger disaster was a fatal incident in the United States space program that occurred on Tuesday, January 28, 1986, when the Space Shuttle Challenger (OV-099) broke apart 73 seconds into its flight, killing all seven crew members aboard. The crew consisted of five NASA astronauts, one payload specialist, and a civilian schoolteacher. The mission carried the designation STS-51-L and was the tenth flight for the Challenger orbiter.
The spacecraft disintegrated over the Atlantic Ocean, off the coast of Cape Canaveral, Florida, at 11:39 a.m. EST (16:39 UTC). The disintegration of the vehicle began after a joint in its right solid rocket booster (SRB) failed at liftoff. The failure was caused by the failure of O-ring seals used in the joint that were not designed to handle the unusually cold conditions that existed at this launch. The seals’ failure caused a breach in the SRB joint, allowing pressurized burning gas from within the solid rocket motor to reach the outside and impinge upon the adjacent SRB aft field joint attachment hardware and external fuel tank. This led to the separation of the right-hand SRB’s aft field joint attachment and the structural failure of the external tank. Aerodynamic forces broke up the orbiter.
Image Credit: NASA
Related Events
Summary
On January 29, 2003, an explosion and fire destroyed the West Pharmaceutical Services plant in Kinston, North Carolina, causing six deaths, dozens of injuries, and hundreds of job losses. The
Summary
On January 29, 2003, an explosion and fire destroyed the West Pharmaceutical Services plant in Kinston, North Carolina, causing six deaths, dozens of injuries, and hundreds of job losses. The facility produced rubber stoppers and other products for medical use. The fuel for the explosion was a fine plastic powder, which accumulated above a suspended ceiling over a manufacturing area at the plant and ignited.
KEY ISSUES:
• HAZARD RECOGNITION & COMMUNICATION
• GOOD ENGINEERING PRACTICE
• LOCAL AMENDMENTS TO FIRE CODES
ROOT CAUSES:
1. West did not perform adequate engineering assessment of the use of powdered zinc stearate and polyethylene as antitack agents in the rubber batchoff process.
2. West engineering management systems did not ensure that relevant industrial fire safety standards were consulted.
3. West management systems for reviewing material safety data sheets did not identify combustible dust hazards.
4. The Kinston plant’s hazard communication program did not identify combustible dust hazards or make the workforce aware of such.
Image Credit: CSB

Summary
On Wednesday, January 29, 2020, a gas well explosion fatally injured three contractors. The gas well was operated by Chesapeake Energy. Image credit: CSB
Summary
On Wednesday, January 29, 2020, a gas well explosion fatally injured three contractors. The gas well was operated by Chesapeake Energy.
Image credit: CSB

Summary
This incident occurred at Synthron, LLC’s Morganton, North Carolina, facility. The company manufactured a variety of powder coating and paint additives by polymerizing acrylic monomers in a 1,500 gallon reactor. The
Summary
This incident occurred at Synthron, LLC’s Morganton, North Carolina, facility. The company manufactured a variety of powder coating and paint additives by polymerizing acrylic monomers in a 1,500 gallon reactor.
The company had received an order for slightly more of an additive than the normal size recipe would produce. Plant managers scaled up the recipe to produce the required larger amount of polymer, and added all of the additional monomer needed into the initial charge to the reactor. This more than doubled the rate of energy release in the reactor, exceeding the cooling capacity of the reactor condenser and causing a runaway reaction.
The reactor pressure increased rapidly. Solvent vapors vented from the reactor’s manway, forming a flammable cloud inside the building. The vapors found an ignition source, and the resulting explosion killed one worker and injured 14. The blast destroyed the facility and damaged off-site structures.
KEY ISSUES:
• REACTIVE HAZARDS & SAFEGUARDS
• CORPORATE OVERSIGHT
• SAFE OPERATING LIMITS
• EVACUATION PLANNING & DRILLS
ROOT CAUSES:
1. A lack of hazard recognition.
2. Poorly documented process safety information & ineffective control of product recipe changes.
3. Lack of automatic safeguards to prevent or mitigate the effects of loss of control over the reaction.
4. Improper manway bolting practices and poor operator training.
5. Inadequate emergency plans drills.
6. Inadequate corporate oversight of process safety.
Image credit: CSB

Related Events
Summary
Three combustible dust incidents over a six month period occurred at the Hoeganaes facility in Gallatin, TN, resulting in fatal injuries to five workers. The facility produces powdered iron and
Summary
Three combustible dust incidents over a six month period occurred at the Hoeganaes facility in Gallatin, TN, resulting in fatal injuries to five workers. The facility produces powdered iron and is located about twenty miles outside of Nashville.
KEY ISSUES:
• HAZARD RECOGNITION AND TRAINING
• ENGINEERING CONTROLS
• FIRE CODES/ENFORCEMENT
• REGULATORY OVERSIGHT
ROOT CAUSES:
1. Hoeganaes facility management were aware of the iron powder combustibility hazard two years prior to the fatal flash fire incidents but did not take necessary action to mitigate the hazard through engineering controls and housekeeping.
2. Hoeganaes did not institute procedures – such as combustible gas monitoring – or training for employees to avoid flammable gas fires and explosions
Image credit: CSB

Summary
Four people were killed in an explosion and fire at an oil gathering center, gas booster station, and power substation. The explosion occurred after a leak from a buried oil
Summary
Four people were killed in an explosion and fire at an oil gathering center, gas booster station, and power substation. The explosion occurred after a leak from a buried oil pipeline in the gathering station spread to a power substation, sparking the blaze. The flash explosion and resulting blaze hit the gathering center and the adjacent gas booster station. At least 19 people were injured in the incident, mainly suffering first- and second-degree burns. The fire was extinguished two days after the event.
[ Property Damage $150 Million. Estimated Current Value $246 Million ]
Image credit: BBC
Summary
A gas leak followed by explosion occurred during an inspection process due to the loose of valve bolt. Proximate causes: • Inadequate training/knowledge transfer (Lack of understanding the process); • Lack
Summary
A gas leak followed by explosion occurred during an inspection process due to the loose of valve bolt.
Proximate causes:
• Inadequate training/knowledge transfer (Lack of understanding the process);
• Lack of work rules/policies/ standards/procedures (wrong procedures for inspections);
• Inadequate work rules plan (lack of the pre-start safety review before inspection).
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: Wikipedia
February
Summary
The Space Shuttle Columbia disaster was a fatal incident in the United States space program that occurred on February 1, 2003, when the Space Shuttle Columbia (OV-102) disintegrated as it
Summary
The Space Shuttle Columbia disaster was a fatal incident in the United States space program that occurred on February 1, 2003, when the Space Shuttle Columbia (OV-102) disintegrated as it re-entered the atmosphere, killing all seven crew members. The disaster was the second fatal accident in the Space Shuttle program, after the 1986 breakup of Challenger soon after liftoff.
During the launch of STS-107, Columbia’s 28th mission, a piece of foam insulation broke off from the Space Shuttle external tank and struck the left wing of the orbiter. Similar foam shedding had occurred during previous shuttle launches, causing damage that ranged from minor to nearly catastrophic, but some engineers suspected that the damage to Columbia was more serious. Before re-entry, NASA managers had limited the investigation, reasoning that the crew could not have fixed the problem if it had been confirmed. When Columbia re-entered the atmosphere of Earth, the damage allowed hot atmospheric gases to penetrate the heat shield and destroy the internal wing structure, which caused the spacecraft to become unstable and break apart.
Image Credit: NASA
Related Events
Summary
On February 2, 2001, a fire occurred at Bethlehem Steel Corporation’s Burns Harbor mill in Chesterton, Indiana. One Bethlehem Steel millwright and one contractor supervisor died. Four Bethlehem Steel millwrights
Summary
On February 2, 2001, a fire occurred at Bethlehem Steel Corporation’s Burns Harbor mill in Chesterton, Indiana. One Bethlehem Steel millwright and one contractor supervisor died. Four Bethlehem Steel millwrights were injured, one seriously. Workers were attempting to remove a slip blind and a cracked valve from a coke oven gas line leading to a decommissioned furnace. During removal of the valve, flammable liquid was released and ignited.
KEY ISSUES:
• MAINTENANCE JOB PLANNING
• FACILITY WINTERIZATION & DEADLEGS
• LINE & EQUIPMENT OPENING
• DECOMMISSIONING & DEMOLITION
ROOT CAUSES:
1. Management systems for the supervision, planning, and execution of maintenance work were inadequate.
2. The Burns Harbor facility did not have a system for monitoring and controlling hazards that could be caused by changes in COG condensate flammability or accumulation rates.
Image Credit: CSB

Summary
On February 7, 2008, at about 7:15 p.m., a series of sugar dust explosions at the Imperial Sugar manufacturing facility in Port Wentworth, Georgia, resulted in 14 worker fatalities. Eight
Summary
On February 7, 2008, at about 7:15 p.m., a series of sugar dust explosions at the Imperial Sugar manufacturing facility in Port Wentworth, Georgia, resulted in 14 worker fatalities. Eight workers died at the scene and six others eventually succumbed to their injuries at the Joseph M. Still Burn Center in Augusta, Georgia. Thirty six workers were treated for serious burns and injuries – some caused permanent, life altering conditions. The explosions and subsequent fires destroyed the sugar packing buildings, palletizer room, and silos, and severely damaged the bulk train car loading area and parts of the sugar refining process areas.
KEY ISSUES:
• COMBUSTIBLE DUST HAZARD RECOGNITION
• MINIMIZING COMBUSTIBLE DUST ACCUMULATION IN THE WORKPLACE
• EQUIPMENT DESIGN & MAINTENANCE
ROOT CAUSES:
1. Sugar and cornstarch conveying equipment was not designed or maintained to minimize the release of sugar and sugar dust into the work area.
2. Inadequate housekeeping practices resulted in significant accumulations of combustible sugar and sugar dust on the floors and elevated surfaces throughout the packing buildings.
3. Imperial Sugar emergency evacuation plans were inadequate. Emergency evacuation drills were not conducted, and prompt worker notification to evacuate in the event of an emergency was inadequate.
Image credit: CSB

Summary
Six workers were fatally injured during a planned work activity to clean debris from natural gas pipes at Kleen Energy in Middletown, CT. To remove the debris, workers used natural
Summary
Six workers were fatally injured during a planned work activity to clean debris from natural gas pipes at Kleen Energy in Middletown, CT. To remove the debris, workers used natural gas at a high pressure of approximately 650 pounds per square inch. The high velocity of the natural gas flow was intended to remove any debris in the new piping. During this process, the natural gas found an ignition source and exploded.
KEY ISSUES:
• SIMILAR NATURAL GAS BLOW INCIDENTS
• INDUSTRY PRACTICES AND SAFER ALTERNATIVE METHODOLOGIES
• HAZARDS OF RELEASING NATURAL GAS NEAR WORK AREAS
• CODES AND STANDARDS
ROOT CAUSES:
1. Natural gas blows are common
2. Workers remained in building during gas blow
Image credit: CSB

Related Events
Summary
On Wednesday, February 8, 2017, at approximately 11:05 am, a foul condensate tank, part of a non-condensable gas system, exploded at the Packaging Corporation of America (PCA) containerboard mill in
Summary
On Wednesday, February 8, 2017, at approximately 11:05 am, a foul condensate tank, part of a non-condensable gas system, exploded at the Packaging Corporation of America (PCA) containerboard mill in DeRidder, Louisiana. The explosion killed three people and injured seven others. All 10 people were working at the mill as contractors. The explosion also heavily damaged the surrounding process. The foul condensate tank travelled approximately 375 feet and over a six-story building before landing on process equipment.
At the time of the incident, the mill was undergoing its annual planned maintenance outage, also referred to as a shutdown. The foul condensate tank likely contained water, a layer of flammable liquid turpentine on top of the water, and an explosive vapor space containing air and flammable turpentine vapor.
KEY ISSUES:
• PROCESS SAFETY MANAGEMENT SYSTEM
• INHERENTLY SAFER DESIGN
• PROCESS HAZARD ANALYSIS
• INEFFECTIVE SAFEGUARDS
• HOT WORK SAFETY MANAGEMENT
ROOT CAUSES:
1. PCA did not evaluate the majority of the non-condensable gas system, including the foul condensate tank, for certain hazards. The DeRidder mill never conducted a process hazard analysis to identify, evaluate, and control process hazards for the non-condensable gas system.
2. PCA did not expand the boundaries of its process safety management program beyond the units covered by safety regulations.
3. PCA did not effectively apply the hierarchy of controls to the selection and implementation of safeguards that the company used to prevent a potential non-condensable gas explosion.
4. PCA did not evaluate inherently safer design options that could have eliminated the possibility of air entering the non-condensable gas system, including the foul condensate tank.
5. PCA did not establish which mill operations group held ownership of, and responsibility for, the foul condensate tank.
6. PCA did not apply important aspects of industry safety guidance and standards.
Image credit: CSB

Summary
An explosion occurred when 8 personnel were working on the repair of a catalyst tower. Proximate causes: • Inadequate training/knowledge transfer (Lack of understanding the process) • Lack of work rules/policies/
Summary
An explosion occurred when 8 personnel were working on the repair of a catalyst tower.
Proximate causes:
• Inadequate training/knowledge transfer (Lack of understanding the process)
• Lack of work rules/policies/ standards/procedures (wrong procedures for inspections);
• Inadequate work rules plan (lack of the pre-start safety review before inspection).
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
Explosion in an oil and gas production ship rented by Petrobras. The explosion occurred aboard the FPSO unit. A leak of flammable substance in the pump room was the cause
Summary
Explosion in an oil and gas production ship rented by Petrobras. The explosion occurred aboard the FPSO unit. A leak of flammable substance in the pump room was the cause of the explosion.
Proximate causes:
• Failure in following procedures
• Lack of work rules/policies/ standards/procedures (breach of operational procedures for the pumping of fluids)
• Inadequate engineering/design
• Inadequate management/ supervision (installation of equipment in pipe without proper technical specification and registration of the change)
• Work exposure to hazardous chemicals (flammable substances) Inadequate assessment of needs and risks
Marsh (https://www.marsh.com/us/insights/research/100-largest-losses-in-the-hydrocarbon-industry.html):
An explosion on a FPSO off the coast of Brazil resulted in nine fatalities and multiple wounded. The accident happened as the vessel was anchored in the Atlantic Ocean 120 kilometres from the coast of Espirito Santos, Brazil. The FPSO is a converted very large crude oil tanker (VLCC), designed to produce up to 10 million cubic meters of natural gas. It is understood that a condensate leak during a fluid transfer operation released a cloud of flammable vapor into the engine room, resulting in an explosion in the machinery space. The majority of fatalities were believed to be part of the emergency response team. FPSO took on water, but the explosion did not result in a breach of the hull of the vessel.
[ Property Damage $250 Million. Estimated Current Value $264 Million ]
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: AFP / Getty Images
Related Events
Summary
An explosion occurred due to an overflow of a slurry mixing tank, containing potassium sulfide, potassium dihydrogen phosphate, and MAP. Proximate causes: • Inadequate training/knowledge transfer (Lack of understanding the process);
Summary
An explosion occurred due to an overflow of a slurry mixing tank, containing potassium sulfide, potassium dihydrogen phosphate, and MAP.
Proximate causes:
• Inadequate training/knowledge transfer (Lack of understanding the process);
• Lack of work rules/policies/ standards/procedures (wrong procedures for inspections);
• Inadequate work rules plan (lack of the pre-start safety review before inspection).
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
A February 20, 2003, dust explosion at the CTA Acoustics, Inc. (CTA) facility in Corbin, Kentucky, killed seven and injured 37 workers. This incident caused extensive damage to the production
Summary
A February 20, 2003, dust explosion at the CTA Acoustics, Inc. (CTA) facility in Corbin, Kentucky, killed seven and injured 37 workers. This incident caused extensive damage to the production area of the 302,000-square-foot plant. Nearby homes and an elementary school were evacuated, and a 12-mile section of Interstate 75 was closed. The largest CTA customer, Ford Motor Company, temporarily suspended operations at four automobile assembly plants because CTA had produced acoustic insulation products for those plants, as well as for other industrial and automotive clients.
KEY ISSUES:
• COMBUSTIBLE DUST HAZARD AWARENESS
• WORK PRACTICES
• BUILDING DESIGN
• PRODUCT STEWARDSHIP
ROOT CAUSES:
1. CTA management did not implement effective measures to prevent combustible dust explosions.
2. The CTA cleaning and maintenance procedures for production lines did not prevent the accumulation of unsafe levels of combustible dust on elevated flat surfaces.
3. The CTA incident investigation program did not ensure that all oven fires were investigated and that underlying causes were identified and resolved.
4. The Borden Chemical product stewardship program did not explicitly convey to CTA the explosive hazards of phenolic resins.
5. The original building design and subsequent building modifications did not effectively address the fire and explosion hazards associated with combustible dusts.
Image Credit: CSB

Summary
On February 23, 1999, a fire occurred in the crude unit at Tosco Corporation. Avon oil refinery in Martinez, California. Workers were attempting to replace piping attached to a 150-foot-tall
Summary
On February 23, 1999, a fire occurred in the crude unit at Tosco Corporation. Avon oil refinery in Martinez, California. Workers were attempting to replace piping attached to a 150-foot-tall fractionator tower while the process unit was in operation. During removal of the piping, naphtha was released onto the hot fractionator and ignited. The flames engulfed five workers located at different heights on the tower. Four men were killed, and one sustained serious injuries.
KEY ISSUES:
• CONTROL OF HAZARDOUS NONROUTINE MAINTENANCE
• MANAGEMENT OVERSIGHT & ACCOUNTABILITY
• MANAGEMENT OF CHANGE
• CORROSION CONTROL
ROOT CAUSES:
1. Tosco Avon refinery’s maintenance management system did not recognize or control serious hazards posed by performing nonroutine repair work while the crude processing unit remained in operation.
2. Tosco’s safety management oversight system did not detect or correct serious deficiencies in the execution of maintenance and review of process changes at its Avon refinery.
Image Credit: CSB

March
Summary
A high-pressure steam (3.7 MPa) discharge occurred during a maintenance process, resulting in three field workers burned to death. Proximate causes: • Lack of work rules/policies/ standards/procedures (wrong procedures for inspections);
Summary
A high-pressure steam (3.7 MPa) discharge occurred during a maintenance process, resulting in three field workers burned to death.
Proximate causes:
• Lack of work rules/policies/ standards/procedures (wrong procedures for inspections);
• Inadequate work rules plan (lack of the pre-start safety review before inspection).
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
At approximately 6:15 p.m. on March 4, 1998, a catastrophic vessel failure and fire occurred near Pitkin, Louisiana, at the Temple 22-1 Common Point Separation Facility owned by Sonat Exploration
Summary
At approximately 6:15 p.m. on March 4, 1998, a catastrophic vessel failure and fire occurred near Pitkin, Louisiana, at the Temple 22-1 Common Point Separation Facility owned by Sonat Exploration Co. Four workers who were near the vessel were killed, and the facility sustained significant damage.
The facility housed two petroleum separation trains and consisted of separation equipment, piping, storage vessels, and a gas distribution system. The separation trains were designed to produce crude oil and natural gas from well fluid, derived from two nearby wells. The vessel ruptured due to overpressurization, releasing flammable material which then ignited.
KEY ISSUES:
• DESIGN & HAZARD REVIEWS
• PRESSURE-RELIEF DEVICES
• OPERATING PROCEDURES
ROOT CAUSES:
1. Sonat management did not use a formal engineering design review process or require effective hazard analyses in the course of designing and building the facility.
2. Sonat engineering specifications did not ensure that equipment that could potentially be exposed to high-pressure hazards was adequately protected by pressure-relief devices.
Image Credit: CSB

Summary
Flooding and capsize of ro-ro passenger ferry Herald of Free Enterprise with loss of 193 lives On the 6th March 1987 the Roll on/Roll off passenger and freight ferry HERALD OF
Summary
Flooding and capsize of ro-ro passenger ferry Herald of Free Enterprise with loss of 193 lives
On the 6th March 1987 the Roll on/Roll off passenger and freight ferry HERALD OF FREE ENTERPRISE (‘HERALD’) under the command of Captain David Lewry sailed from Number 12 berth in the inner harbour at Zeebrugge at 18.05 G.M.T. The HERALD was manned by a crew of 80 hands all told and was laden with 81 cars, 47 freight vehicles and three other vehicles.
Approximately 459 passengers had embarked for the voyage to Dover, which they expected to be completed without incident in the prevailing good weather. There was a light easterly breeze and very little sea or swell. The HERALD passed the outer mole at 18.24. She capsized about four minutes later. During the final moments the HERALD turned rapidly to starboard and was prevented from sinking totally by reason only that her port side took the ground in shallow water. The HERALD came to rest on a heading of 136° with her starboard side above the surface. Water rapidly filled the ship below the surface level with the result that not less than 150 passengers and 38 members of the crew lost their lives. Many others were injured.
Image Credit: Independent
Summary
A hairline crack in a welded seam of piping to the level indicator system on an aldehyde column resulted in a minor ethylene oxide leak on this gas processing plant.
Summary
A hairline crack in a welded seam of piping to the level indicator system on an aldehyde column resulted in a minor ethylene oxide leak on this gas processing plant. As a result of this crack, which was caused by low cycle fatigue, ethylene oxide escaped near the level indicator and formed polyethylene glycols (PEG) in the mineral wool insulation. It is believed that both the leak and accumulation of PEG occurred over a period of time. During repairs to the level indicator, the metal sheathing of the insulation was removed and air contacted the insulation soaked with PEG. Auto-oxidation of the PEG resulted and the insulating material was ignited. The piping to the level indicator system was heated to such a degree that auto-decomposition of the ethylene oxide within the piping occurred. This autodecomposition propagated into the aldehyde column which subsequently exploded. The force of the explosion completely destroyed the distillation section of this plant. The large resulting fire and impact of flying debris to other process sections resulted in extensive damage throughout the plant.
[ Property Damage $79 Million. Estimated Current Value $178 Million ]
Image credit: No credit
Summary
On March 11, 2011, the Great East Japan Earthquake triggered an extremely severe nuclear accident at the Fukushima Daiichi Nuclear Power Plant, owned and operated by the Tokyo Electric Power
Summary
On March 11, 2011, the Great East Japan Earthquake triggered an extremely severe nuclear accident at the Fukushima Daiichi Nuclear Power Plant, owned and operated by the Tokyo Electric Power Company (TEPCO). This devastating accident was ultimately declared a Level 7 (“Severe Accident”) by the International Nuclear Event Scale (INES).
When the earthquake occurred, Unit 1 of the Fukushima Daiichi plant was in normal operation at the rated electricity output according to its specifications; Units 2 and 3 were in operation within the rated heat parameters of their specifications; and Units 4 to 6 were undergoing periodical inspections. The emergency shut-down feature, or SCRAM, went into operation at Units 1, 2 and 3 immediately after the commencement of the seismic activity.
Although there were no immediate fatalities, a worker later died from radiation exposure (https://www.reuters.com/article/us-japan-fukushima-radiation/japan-acknowledges-first-radiation-death-among-fukushima-workers-idUSKCN1LL0OA)
Image Credit: NY Times
Topics
Summary
A gas leak involving the pipe rack that runs to the terminal of this petrochemical complex led to an explosion, which occurred near the complex chemical plant, causing additional damage
Summary
A gas leak involving the pipe rack that runs to the terminal of this petrochemical complex led to an explosion, which occurred near the complex chemical plant, causing additional damage to the pipe rack and resulting in a major gas leak. A powerful second explosion occurred that could be felt more than 15 miles from the complex. These explosions and a subsequent fire completely destroyed the chemical plant, caused significant damage to the pipe rack, and resulted in moderate damage to other complex buildings and adjacent third-party facilities. The fire was extinguished after approximately three hours. Because of this incident, the chemical plant at this complex was completely shut down for seven months to allow for the rebuild of the plant and the pipe rack.
[ Property Damage $97 Million. Estimated Current Value $208 Million ]
Image credit: Reuters
Summary
An explosion occurred in the ethylene oxide process unit at this plant. As a result, the ethylene oxide refining column was completely destroyed, the ethylene glycol unit was substantially damaged,
Summary
An explosion occurred in the ethylene oxide process unit at this plant. As a result, the ethylene oxide refining column was completely destroyed, the ethylene glycol unit was substantially damaged, and the co-generation unit was partially damaged. A pipe rack near the storage area for liquid ethylene oxide was damaged when a large piece of shrapnel from the explosion hit the rack, rupturing lines which contained methane and other hydrocarbon products.
The subsequent fire that resulted from the released products was the only significant fire to occur during this incident. As a result of the explosion, all utilities at the plant were lost for approximately one week. Additionally, several fixed fire protection systems were damaged by the explosion or inadvertently actuated due to a loss of plant air. These systems were shut off, isolated, or placed back in service, as appropriate. A manual fire fighting effort was used to extinguish the fire in the pipe rack once the lines in the rack were isolated. The polyethylene production was restarted in early April 1991 using imported ethylene. The olefins production unit was restarted in late April 1991.
[ Property Damage $90 Million. Estimated Current Value $194 Million ]
Image credit: Vitaly Shmatikov
Summary
Fifteen months before the incident occurred it had been noticed that the flare line isolation valve V17 was passing. It was decided however to wait for a scheduled shutdown of
Summary
Fifteen months before the incident occurred it had been noticed that the flare line isolation valve V17 was passing. It was decided however to wait for a scheduled shutdown of the catalytic cracker unit and No 1 flare before commencing work on the valve. Gases from the remaining operating units were re-routed to No 2 and No 3 flares. This flare arrangement would allow the pipelines at V17 to be isolated.
When senior refinery staff prepared a plan for the isolation of the flare system, they concentrated on the operational and safety requirements of the flare system, making sure that no operational areas of the plant were inadvertently isolated. The details of the removal of V17 were not considered and left to those who would be responsible for the work.
Four workers were involved with the removal of the valve. When the majority of the bolts were undone the joint opened slightly and liquid dripped from a small gap between the flanges. The workers sought advice. The valve was checked and it was concluded that it was safe to carry on. Non ferrous hammers were provided before continuing with the removal. All the bolts were removed and the crane took the weight of a spacer and started to remove it, at which point gallons of liquid poured from the valve. A flammable vapour cloud formed from the rapidly spreading pool. The cloud reached the nearby air compressor, ignited and flashed back around the working area.
Two workers managed to escape the fire but a fitter and a rigger were engulfed by the flames and killed. The fire was allowed to burn in a controlled manner for almost two days while the rest of the refinery was shut down and the flare system purged with nitrogen
KEY ISSUES:
• DESIGN CODES – PIPEWORK
• MAINTENANCE PROCEDURES
• ISOLATION
Report: https://www.icheme.org/media/13700/the-fires-and-explosion-at-bp-oil-grangemouth-refinery-ltd.pdf
Image Credit: HSE
Summary
On March 13, 2001, three people were killed as they opened a process vessel containing hot plastic at the BP Amoco Polymers plant in Augusta, Georgia. They were unaware that
Summary
On March 13, 2001, three people were killed as they opened a process vessel containing hot plastic at the BP Amoco Polymers plant in Augusta, Georgia. They were unaware that the vessel was pressurized. The workers were killed when the partially unbolted cover blew off the vessel, expelling hot plastic. The force of the release caused some nearby tubing to break. Hot fluid from the tubing ignited, resulting in a fire.
KEY ISSUES:
• RECOGNITION OF REACTIVE HAZARDS
• LEARNING FROM NEAR-MISS INCIDENTS
• OPENING OF PROCESS EQUIPMENT
ROOT CAUSES:
1. Amoco, the developer of the Amodel process, did not adequately review the conceptual process design to identify chemical reaction hazards.
2. The Augusta facility did not have an adequate review process for correcting design deficiencies.
3. The Augusta site system for investigating incidents and nearmiss incidents did not adequately identify causes or related hazards. This information was needed to correct the design and operating deficiencies that led to the recurrence of incidents.
Image Credit: CSB

Related Events
Summary
The world’s largest offshore production facility was rocked by a series of explosions caused by a gas release. The explosions knocked out a support pillar of the semi-submersible platform allowing
Summary
The world’s largest offshore production facility was rocked by a series of explosions caused by a gas release. The explosions knocked out a support pillar of the semi-submersible platform allowing seawater to enter the vessel. Workers pumped in nitrogen and compressed air and tried to pump out almost 3,000 metric tons of seawater to keep the rig afloat, but were unsuccessful. On March 20, 2001, the rig sank to the sea floor. The incident killed 11 workers.
[ Property Damage $500 Million. Estimated Current Value $851 Million ]
Ref: http://www.anp.gov.br/noticias/2342-anp-marinha-comissao-conjunta
Image credit: Petrobras
Related Events
Summary
An explosion occurred when 6 personnel were working on the repair of a catalyst tower Proximate causes: • Lack of work rules/policies/ standards/procedures (wrong procedures for inspections); • Inadequate work
Summary
An explosion occurred when 6 personnel were working on the repair of a catalyst tower
Proximate causes:
• Lack of work rules/policies/ standards/procedures (wrong procedures for inspections);
• Inadequate work rules plan (lack of the pre-start safety review before inspection).
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
Contract personnel were installing a pig trap on an 18-inch-diameter export gas pipeline on the platform. As a cold cut was made into the pipeline, hydrocarbons sprayed from the cut
Summary
Contract personnel were installing a pig trap on an 18-inch-diameter export gas pipeline on the platform. As a cold cut was made into the pipeline, hydrocarbons sprayed from the cut and ignited. The explosion and fire burned the main structure and caused subsequent explosions when six other pipelines ruptured due to the intense heat. The accident resulted in the total destruction of the platform and seven fatalities. It took two years to replace the platform.
[ Property Damage $400 Million. Estimated Current Value $899 Million ]
Image credit: ARCO
Summary
On 20 March 1990 the halogen exchange reactor on the Fluoroaromatics plant was ruptured by the pressure generated by a runaway reaction. The plant was partially destroyed and missiles were
Summary
On 20 March 1990 the halogen exchange reactor on the Fluoroaromatics plant was ruptured by the pressure generated by a runaway reaction. The plant was partially destroyed and missiles were projected over 500m. Six employees were injured and one subsequently died from post-operative complications.
A batch had been charged into the vessel and was being heated up as normal. When it reached 165oC, the temperature continued to rise and the operators adjusted the jacket temperature. The display screen in use did not display pressure and they were unaware of a corresponding rise in pressure. By the time they were alerted to the rise in pressure the pressure relief valves had lifted. Before any other corrective action could be taken, the reactor exploded. The pressure in the vessel reached a value of about 60-80 barg compared with the relief valve set pressure of 5 barg.
The resulting blast was enhanced by the formation of a fireball, which occurred when the contents of the reactor ignited within the plant structure. This started local fires and initiated what became a major conflagration in an adjacent unit where vessels containing xylene were damaged by the blast/missile effects. The ensuing fires were brought under control in four hours by the Shell fire team and Cheshire fire service.
The initial cause of the incident was the ingress of excessive water into the process leading to the formation of acetic acid which, upon recycle to the reactor, reacted vigorously with the reactor contents initiating the explosion. Water was present as a part of the process, however a massive incursion led to the formation of a separate layer in the process vessel which was not removed but recycled back into reactor.
KEY ISSUES:
• CONTROL ROOM DESIGN
• RAW MATERIALS CONTROL / SAMPLING
• REACTION / PRODUCT TESTING
• RELIEF SYSTEMS / VENT SYSTEMS
Image Credit: The Leader
Summary
On March 21, 2011, during calcium carbide production at the Carbide Industries plant in Louisville, KY, an electric arc furnace exploded, ejecting solid and powdered debris, flammable gases, and molten
Summary
On March 21, 2011, during calcium carbide production at the Carbide Industries plant in Louisville, KY, an electric arc furnace exploded, ejecting solid and powdered debris, flammable gases, and molten calcium carbide at temperatures near 3800°F (2100°C). Two workers died and two others were injured.
KEY ISSUES:
• FACILITY SITING
• NORMALIZATION OF DEVIANCE
• CONSENSUS STANDARDS
ROOT CAUSES:
1. Despite past incidents, neither the previous owners nor Carbide Industries identified that the control room should be relocated and cameras installed to better protect workers while they remotely monitored the furnace.
2. Carbide Industries issued 26 work orders for leak repair for water leaks on the furnace cover in the five months prior to the March 2011 incident, but continued operating the furnace despite the hazard from ongoing water leaks.
3. The company did not adequately address past explosive incidents, which normalized blows as routine events.
4. The company did not have a process safety management program in place that required the elimination of overpressure incidents in the furnace.
Image credit: CSB

Summary
On Saturday 21 March 1987 the hydrocracker unit was being recommissioned following a routine shut down. During the recommissioning a plant trip occurred. This was thought to be a spurious
Summary
On Saturday 21 March 1987 the hydrocracker unit was being recommissioned following a routine shut down. During the recommissioning a plant trip occurred. This was thought to be a spurious trip and the plant operators started to bring up the unit to normal operating conditions. From then on until the time of the incident the plant was held in stand by condition with no fresh feed.
At 07:00 hours the following morning there was a violent explosion and subsequent fire. The explosion could be heard and felt up to 30km away. The explosion centred on a low pressure (LP) separator vessel, V306, which was fabricated from 18mm steel plate and weighed 20 tonnes.
The investigation of the accident suggested that an air operated control valve on the high pressure (HP) separator had been opened and closed on manual control at least three times. Liquid level in the LP separator fell and the valve was opened. This action allowed the remaining liquid in the HP separator to drain away and for high pressure gas to break through into the LP separator. As the pressure relief on the LP separator had been designed for a fire relief case, not gas breakthrough the vessel subsequently exploded.
The control valve did not close automatically because the low low level trip on the HP separator had been disconnected several years earlier. The operators did not trust the main level control reading and referred to a chart recorder for a back up level reading. There was an offset on this chart recorder which led them to assume that the level in the HP separator was normal.
KEY ISSUES:
• MAINTENANCE PROCEDURES
• CONTROL SYSTEMS
• OPERATING PROCEDURES
• PLANT MODIFICATION / CHANGE PROCEDURES
• ALARM / TRIPS / INTERLOCKS
• RELIEF SYSTEMS / VENT SYSTEMS
• ISOLATION
Report: https://www.icheme.org/media/13700/the-fires-and-explosion-at-bp-oil-grangemouth-refinery-ltd.pdf
Image Credit: HSE
Summary
At approximately 1:20 p.m. on March 23, 2005, a series of explosions occurred at the BP Texas City refinery during the restarting of a hydrocarbon isomerization unit. Fifteen workers were
Summary
At approximately 1:20 p.m. on March 23, 2005, a series of explosions occurred at the BP Texas City refinery during the restarting of a hydrocarbon isomerization unit. Fifteen workers were killed and 180 others were injured. Many of the victims were in or around work trailers located near an atmospheric vent stack. The explosions occurred when a distillation tower flooded with hydrocarbons and was overpressurized, causing a geyser-like release from the vent stack.
KEY ISSUES:
• SAFETY CULTURE
• REGULATORY OVERSIGHT
• PROCESS SAFETY METRICS
• HUMAN FACTORS
ROOT CAUSES:
1. BP Group Board did not provide effective oversight of the company’s safety culture and major accident prevention programs.
2. Senior executives:
• inadequately addressed controlling major hazard risk. Personal safety was measured, rewarded, and the primary focus, but the same emphasis was not put on improving process safety performance;
• did not provide effective safety culture leadership and oversight to prevent catastrophic accidents;
• ineffectively ensured that the safety implications of major organizational, personnel, and policy changes were evaluated;
• did not provide adequate resources to prevent major accidents; budget cuts impaired process safety performance at the Texas City refinery.
3. BP Texas City Managers did not:
• create an effective reporting and learning culture; reporting bad news was not encouraged. Incidents were often ineffectively investigated and appropriate corrective actions not taken.
• ensure that supervisors and management modeled and enforced use of up-to-date plant policies and procedures.
• incorporate good practice design in the operation of the ISOM unit.
• ensure that operators were supervised and supported by experienced, technically trained personnel during unit startup, an especially hazardous phase of operation; or that
• effectively incorporated human factor considerations in its training, staffing, and work schedule for operations personnel.
Image Credit: CSB

Related Events
Topics
Summary
An apparent failure of a propane intercooler liquid level control during unsupervised maintenance led to an explosion and fire. The control room on the main platform was destroyed and adjacent
Summary
An apparent failure of a propane intercooler liquid level control during unsupervised maintenance led to an explosion and fire. The control room on the main platform was destroyed and adjacent platforms were affected by the blast wave. There were 11 fatalities.
[ Property Damage $100 Million. Estimated Current Value $194 Million ]
Image credit: PDVSA
Summary
The Alexander L Kielland was a semi-submersible platform accommodating the workers of the bridge-linked Edda oil rig in the Ekofisk field, approximately 235 miles east of Dundee, Scotland, in the
Summary
The Alexander L Kielland was a semi-submersible platform accommodating the workers of the bridge-linked Edda oil rig in the Ekofisk field, approximately 235 miles east of Dundee, Scotland, in the Norwegian Continental Shelf. The Phillips Petroleum-operated platform capsized in March 1980, killing 123 people.
Only 89 out of 212 workers survived the accident and most died by drowning as the platform turned upside-down in deep waters. The platform capsized after the failure of one of the bracings attached to one leg of the five-legged platform structure after strong winds created waves of up to 12 m high on the day of the accident.
Ref: https://en.wikipedia.org/wiki/Alexander_L._Kielland_(platform)
Image Credit: Norwegian Petroleum Museum
Summary
On March 27, 1998, at approximately 12:15 pm, two workers at Union Carbide Corporation’s Taft/Star Manufacturing Plant (the plant) in Hahnville, Louisiana, were overcome by nitrogen gas while performing a
Summary
On March 27, 1998, at approximately 12:15 pm, two workers at Union Carbide Corporation’s Taft/Star Manufacturing Plant (the plant) in Hahnville, Louisiana, were overcome by nitrogen gas while performing a black light inspection at an open end of a 48-inch-wide horizontal pipe. The 48-inch pipe was open because chemical-processing equipment had been shut down and opened for major maintenance. Nitrogen was being injected into the process equipment primarily to protect new catalyst in reactors from exposure to moisture. The nitrogen was also flowing through some of the piping systems connected to the reactors. The nitrogen was venting from one side of the open pipe where it had formerly been connected to an oxygen feed mixer. No warning sign was posted on the pipe opening identifying it as a confined space or warning that the pipe contained potentially hazardous nitrogen.
The two workers had placed a sheet of black plastic over the end of the pipe to provide shade to make it easier to conduct the black light test during daylight. While working just outside the pipe opening and inside of the black plastic sheet, the two workers were overcome by nitrogen. One worker died from asphyxiation. The other worker survived but was severely injured.
KEY ISSUES:
• USE OF NITROGEN IN CONFINED SPACES
• SAFETY OF TEMPORARY ENCLOSURES
ROOT CAUSES:
1. Procedures to control potential hazards created by erecting temporary enclosures around nitrogen-containing equipment were inadequate.
2. Nitrogen and confined space hazard warnings were inadequate.
Image Credit: CSB

Summary
A major explosion in a firecracker unit occurred. The unit was run illegally by the owner who was later taken under custody. Explosions in firecracker units have been a prevalent
Summary
A major explosion in a firecracker unit occurred. The unit was run illegally by the owner who was later taken under custody. Explosions in firecracker units have been a prevalent problem in the state of Seemandhra, India which needs to be addressed.
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: PTI