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February
Summary
At about 8.23 pm on 1 February 1994 there was a release of reactor solution from a recirculating pump near the base of a 25 tonne ethyl chloride (EC) reactor
Summary
At about 8.23 pm on 1 February 1994 there was a release of reactor solution from a recirculating pump near the base of a 25 tonne ethyl chloride (EC) reactor vessel at the factory of The Associated Octel Company Ltd, Ellesmere Port, Cheshire. The reactor solution was highly flammable, corrosive and toxic, mainly consisting of ethyl chloride, a liquefied flammable gas, mixed with hydrogen chloride a toxic and corrosive gas, and small quantities of solid catalyst, aluminium chloride. A dense, white cloud soon enveloped the plant and began to move off-site.
The on-site and external emergency services were called in accordance with pre-arranged procedures for major incidents involving chemical release. Over the next one and a half hours action was taken to isolate the leak, to suppress the further release of vapour and to prevent the cloud spreading.
In spite of these attempts a pool of liquid continued to collect and at 10.08 pm the flammable vapours of ethyl chloride ignited, causing a major pool fire which was most intense at the base of the reactor. As the incident developed there were also fires at flanges damaged in the fire, including jet flames at the top of two large process vessels on the plant. Although these vessels and the reactor were protected by a fire resistant coating, there was concern at one stage that the vessels might explode and the damage extend to chlorine storage vessels on the adjacent plant.
The leak occurred at a point between fixed pipework and the discharge port of a pump recirculating liquids to the reactor, as a direct consequence of either (a) the failure of a corroded securing flange on the pump working loose; or (b) the failure of a PTFE flexible connection (‘bellows’) connecting the pump discharge to the pipe. The HSE believes the first of these possible causes was the more likely. The most likely source of ignition was an electrical control box to a compressor nearby.
KEY ISSUES:
• CORROSION / SELECTION OF MATERIALS
• DESIGN CODES – PIPEWORK
• MAINTENANCE PROCEDURES
• ISOLATION
Image Credit: HSE
Summary
On February 2, 2001, a fire occurred at Bethlehem Steel Corporation’s Burns Harbor mill in Chesterton, Indiana. One Bethlehem Steel millwright and one contractor supervisor died. Four Bethlehem Steel millwrights
Summary
On February 2, 2001, a fire occurred at Bethlehem Steel Corporation’s Burns Harbor mill in Chesterton, Indiana. One Bethlehem Steel millwright and one contractor supervisor died. Four Bethlehem Steel millwrights were injured, one seriously. Workers were attempting to remove a slip blind and a cracked valve from a coke oven gas line leading to a decommissioned furnace. During removal of the valve, flammable liquid was released and ignited.
KEY ISSUES:
• MAINTENANCE JOB PLANNING
• FACILITY WINTERIZATION & DEADLEGS
• LINE & EQUIPMENT OPENING
• DECOMMISSIONING & DEMOLITION
ROOT CAUSES:
1. Management systems for the supervision, planning, and execution of maintenance work were inadequate.
2. The Burns Harbor facility did not have a system for monitoring and controlling hazards that could be caused by changes in COG condensate flammability or accumulation rates.
Image Credit: CSB

Summary
Heavy storm conditions in the North Sea caused four of this floating production, storage, and offloading’s (FPSO) 10 anchor chains to break resulting in the vessel moving off its position.
Summary
Heavy storm conditions in the North Sea caused four of this floating production, storage, and offloading’s (FPSO) 10 anchor chains to break resulting in the vessel moving off its position. It is estimated that the FPSO was subject to 53-knot winds and nine meter waves. Normally, a complex piping system runs from the wells on the seabed up to the FPSO, however, this infrastructure was damaged in the incident. Following the vessel moving off its position, all of the wells were immediately shut in. Subsequent surveys showed that no oil had been lost. The 74 non-essential crew were evacuated to near-by platforms and 43 essential crew members remained onboard. Two members of crew received minor injuries. The facility was projected to be producing an average of 18,400 bbl-per-day of oil prior to the loss.
[ Property Damage $450 Million. Estimated Current Value $497 Million ]
Image credit: Maersk
Summary
A tank ruptured in Warsaw Chemical company, it contained hazardous chemical that caused a fire followed by an explosion. After the fire some chemicals spilled into Winona lake. 50 homes were
Summary
A tank ruptured in Warsaw Chemical company, it contained hazardous chemical that caused a fire followed by an explosion. After the fire some chemicals spilled into Winona lake.
50 homes were evacuated
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: 1480 News Now
Summary
On February 7, 2008, at about 7:15 p.m., a series of sugar dust explosions at the Imperial Sugar manufacturing facility in Port Wentworth, Georgia, resulted in 14 worker fatalities. Eight
Summary
On February 7, 2008, at about 7:15 p.m., a series of sugar dust explosions at the Imperial Sugar manufacturing facility in Port Wentworth, Georgia, resulted in 14 worker fatalities. Eight workers died at the scene and six others eventually succumbed to their injuries at the Joseph M. Still Burn Center in Augusta, Georgia. Thirty six workers were treated for serious burns and injuries – some caused permanent, life altering conditions. The explosions and subsequent fires destroyed the sugar packing buildings, palletizer room, and silos, and severely damaged the bulk train car loading area and parts of the sugar refining process areas.
KEY ISSUES:
• COMBUSTIBLE DUST HAZARD RECOGNITION
• MINIMIZING COMBUSTIBLE DUST ACCUMULATION IN THE WORKPLACE
• EQUIPMENT DESIGN & MAINTENANCE
ROOT CAUSES:
1. Sugar and cornstarch conveying equipment was not designed or maintained to minimize the release of sugar and sugar dust into the work area.
2. Inadequate housekeeping practices resulted in significant accumulations of combustible sugar and sugar dust on the floors and elevated surfaces throughout the packing buildings.
3. Imperial Sugar emergency evacuation plans were inadequate. Emergency evacuation drills were not conducted, and prompt worker notification to evacuate in the event of an emergency was inadequate.
Image credit: CSB

Summary
A February 7, 2003, explosion and fire inside a vent collection system (VCS) at Technic Inc., in Cranston, Rhode Island, critically injured one employee, who suffered permanent eye damage and
Summary
A February 7, 2003, explosion and fire inside a vent collection system (VCS) at Technic Inc., in Cranston, Rhode Island, critically injured one employee, who suffered permanent eye damage and chemical burns to his face and upper body. Eighteen other employees were sent to the hospital for medical evaluations, and the fire department evacuated the surrounding community. Facility operations were interrupted for several weeks.
The explosion and fire were caused by a violent chemical reaction inside the vent collection system, which was likely initiated when the employee tapped on a duct with a small hammer. The building where the incident occurred housed several chemical processes that were connected to the ventilation system.
KEY ISSUES:
• INCOMPATIBLE CHEMICAL MIXING
• PROCESS SAFETY REVIEW
• MANAGEMENT OF CHANGE
• PREVENTIVE MAINTENANCE
• EMERGENCY PLANNING & RESPONSE
ROOT CAUSES:
1. Technic did not conduct a process safety review as a part of the engineering process to identify and evaluate the hazards associated with installing a vent collection system to handle the exhausts from multiple processes.
2. Technic did not identify and evaluate the hazards created by changes to facility processes and equipment (i.e., management of change).
Image Credit: CSB

Summary
Six workers were fatally injured during a planned work activity to clean debris from natural gas pipes at Kleen Energy in Middletown, CT. To remove the debris, workers used natural
Summary
Six workers were fatally injured during a planned work activity to clean debris from natural gas pipes at Kleen Energy in Middletown, CT. To remove the debris, workers used natural gas at a high pressure of approximately 650 pounds per square inch. The high velocity of the natural gas flow was intended to remove any debris in the new piping. During this process, the natural gas found an ignition source and exploded.
KEY ISSUES:
• SIMILAR NATURAL GAS BLOW INCIDENTS
• INDUSTRY PRACTICES AND SAFER ALTERNATIVE METHODOLOGIES
• HAZARDS OF RELEASING NATURAL GAS NEAR WORK AREAS
• CODES AND STANDARDS
ROOT CAUSES:
1. Natural gas blows are common
2. Workers remained in building during gas blow
Image credit: CSB

Related Events
Summary
On Wednesday, February 8, 2017, at approximately 11:05 am, a foul condensate tank, part of a non-condensable gas system, exploded at the Packaging Corporation of America (PCA) containerboard mill in
Summary
On Wednesday, February 8, 2017, at approximately 11:05 am, a foul condensate tank, part of a non-condensable gas system, exploded at the Packaging Corporation of America (PCA) containerboard mill in DeRidder, Louisiana. The explosion killed three people and injured seven others. All 10 people were working at the mill as contractors. The explosion also heavily damaged the surrounding process. The foul condensate tank travelled approximately 375 feet and over a six-story building before landing on process equipment.
At the time of the incident, the mill was undergoing its annual planned maintenance outage, also referred to as a shutdown. The foul condensate tank likely contained water, a layer of flammable liquid turpentine on top of the water, and an explosive vapor space containing air and flammable turpentine vapor.
KEY ISSUES:
• PROCESS SAFETY MANAGEMENT SYSTEM
• INHERENTLY SAFER DESIGN
• PROCESS HAZARD ANALYSIS
• INEFFECTIVE SAFEGUARDS
• HOT WORK SAFETY MANAGEMENT
ROOT CAUSES:
1. PCA did not evaluate the majority of the non-condensable gas system, including the foul condensate tank, for certain hazards. The DeRidder mill never conducted a process hazard analysis to identify, evaluate, and control process hazards for the non-condensable gas system.
2. PCA did not expand the boundaries of its process safety management program beyond the units covered by safety regulations.
3. PCA did not effectively apply the hierarchy of controls to the selection and implementation of safeguards that the company used to prevent a potential non-condensable gas explosion.
4. PCA did not evaluate inherently safer design options that could have eliminated the possibility of air entering the non-condensable gas system, including the foul condensate tank.
5. PCA did not establish which mill operations group held ownership of, and responsibility for, the foul condensate tank.
6. PCA did not apply important aspects of industry safety guidance and standards.
Image credit: CSB

Summary
An explosion occurred when 8 personnel were working on the repair of a catalyst tower. Proximate causes: • Inadequate training/knowledge transfer (Lack of understanding the process) • Lack of work rules/policies/
Summary
An explosion occurred when 8 personnel were working on the repair of a catalyst tower.
Proximate causes:
• Inadequate training/knowledge transfer (Lack of understanding the process)
• Lack of work rules/policies/ standards/procedures (wrong procedures for inspections);
• Inadequate work rules plan (lack of the pre-start safety review before inspection).
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
On the 11 February 1980 a fire and a series of explosions occurred at a warehouse in a factory at Trubshaw Cross, Longport, Stoke-on-Trent. On the morning of the fire
Summary
On the 11 February 1980 a fire and a series of explosions occurred at a warehouse in a factory at Trubshaw Cross, Longport, Stoke-on-Trent. On the morning of the fire the warehouse contained some 49 tonnes of liquefied petroleum gas (LPG) in cartridges and aerosol containers as well as about 1 tonne of petroleum mixtures in small containers, raw materials, and packaging materials. It is almost certain that the source of ignition was the electrical system of a battery operated fork lift truck.
LPG is a well known fire and explosion hazard; the circumstances of the fire emphasise the need for occupiers of premises containing LPG to be adequately informed, by obtaining information and advice from authoritative sources, on the hazards of LPG and the precautions to be observed in its storage.
Report: https://www.icheme.org/media/13695/the-fire-and-explosions-at-permaflex-trubshaw-cross-stoke.pdf
Image Credit: Stoke Sentinel
Summary
The main turret bearing on a FPSO vessel seized and subsequently failed, resulting in the vessel being unable to weathervane. Production was resumed with a revised operating regime employing tugs
Summary
The main turret bearing on a FPSO vessel seized and subsequently failed, resulting in the vessel being unable to weathervane. Production was resumed with a revised operating regime employing tugs to maintain a constant heading. Subsequently, the vessel was converted to employ a permanent spread moored configuration, fixing the heading of the vessel and installing an associated deepwater offloading buoy.
[ Property Damage $450 Million. Estimated Current Value $466 Million ]
Image credit: Tullow Oil
Summary
Explosion in an oil and gas production ship rented by Petrobras. The explosion occurred aboard the FPSO unit. A leak of flammable substance in the pump room was the cause
Summary
Explosion in an oil and gas production ship rented by Petrobras. The explosion occurred aboard the FPSO unit. A leak of flammable substance in the pump room was the cause of the explosion.
Proximate causes:
• Failure in following procedures
• Lack of work rules/policies/ standards/procedures (breach of operational procedures for the pumping of fluids)
• Inadequate engineering/design
• Inadequate management/ supervision (installation of equipment in pipe without proper technical specification and registration of the change)
• Work exposure to hazardous chemicals (flammable substances) Inadequate assessment of needs and risks
Marsh (https://www.marsh.com/us/insights/research/100-largest-losses-in-the-hydrocarbon-industry.html):
An explosion on a FPSO off the coast of Brazil resulted in nine fatalities and multiple wounded. The accident happened as the vessel was anchored in the Atlantic Ocean 120 kilometres from the coast of Espirito Santos, Brazil. The FPSO is a converted very large crude oil tanker (VLCC), designed to produce up to 10 million cubic meters of natural gas. It is understood that a condensate leak during a fluid transfer operation released a cloud of flammable vapor into the engine room, resulting in an explosion in the machinery space. The majority of fatalities were believed to be part of the emergency response team. FPSO took on water, but the explosion did not result in a breach of the hull of the vessel.
[ Property Damage $250 Million. Estimated Current Value $264 Million ]
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: AFP / Getty Images
Related Events
Summary
At approximately 10:00 hours workers on site noticed the electrical lights flickering and saw smoke coming from the warehouse. On opening the warehouse door to investigate, a wall of thick
Summary
At approximately 10:00 hours workers on site noticed the electrical lights flickering and saw smoke coming from the warehouse. On opening the warehouse door to investigate, a wall of thick smoke confronted an employee. Shutting the door he raised the alarm and called the fire brigade. The warehouse was used for storing large quantities of ICI herbicides in plastic bottles and drums with plastic liners and octyl phenol in paper sacks.
The fire brigade responded promptly and was automatically issued with TREM cards (Transport Emergency Cards) relating to the herbicides and Octyl Phenol. However, by this time the fire had become established and had broken through the roof of the warehouse. The intensity and speed at which the fire developed surprised the fire fighters, as they believed the warehouse contents to be largely incombustible.
Some of the drums/bottles had burst in the fire and their contents were washed down the road and into Hey Beck, a small stream that drains from the site. This resulted in a major pollution incident. Because of the large volumes involved the decision was taken to allow the material to continue to flow into the drains, washed down by the fire brigade. This washing down activity continued for over two days after the incident. The diluted herbicides turned the stream into a brown foaming torrent for several miles. The River Calder was affected by this pollution. The fire fighters were faced with additional problems because of the physical properties of octyl phenol. This substance floats on water producing a flowing pool of burning liquid.
The seriousness of the pollution prompted action to be taken to contact police, the water authority, local radio stations and the press to warn the general public of the dangers of coming into contact with the contaminated water. Farmers were warned to keep livestock away from riverbanks.
The exact cause of this accident is unknown. A worker had been shrink-wrapping paper sacks of octyl phenol onto wooden pallets using a plastic film and a hand held cylinder heat gun, shortly before the incident occurred. It is feasible that the flame from the gun passing too close overheated one of the pallets, causing one or more bags, or the pallet to smoulder, eventually bursting in flames.
KEY ISSUES:
• EMERGENCY RESPONSE / SPILL CONTROL
• REACTION / PRODUCT TESTING
Image Credit: West Yorkshire Fire & Rescue Service
Summary
A rail car with more than 100 tanks of crude bakken oil derailed in West Virginia, generating a huge fireball, the evacuation of hundreds of people and, a spill into
Summary
A rail car with more than 100 tanks of crude bakken oil derailed in West Virginia, generating a huge fireball, the evacuation of hundreds of people and, a spill into the Kanawha River.
Hundreds evacuated – FRE issued CSX and Sperry Rail Service $25.000 fines each
Proximate causes:
• Inadequate tools, equipment & vehicles (rail defect)
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: US Coast Guard
Summary
At 2:09 p.m. on Friday, February 16, 2007, liquid propane under high pressure was released in the Propane De-Asphalting (PDA) unit of Valero’s McKee Refinery, 50 miles north of Amarillo
Summary
At 2:09 p.m. on Friday, February 16, 2007, liquid propane under high pressure was released in the Propane De-Asphalting (PDA) unit of Valero’s McKee Refinery, 50 miles north of Amarillo in the Texas panhandle, near the town of Sunray. The resulting propane vapor cloud found an ignition source, and the subsequent fire injured workers, damaged unit piping and equipment, and collapsed a major piperack. The fire grew rapidly and threatened surrounding units, including a Liquefied Petroleum Gas (LPG) storage area. Fire-fighting efforts were hampered by high and shifting winds and the rapid spread of the fire. A refinery-wide evacuation was ordered approximately 15 minutes after the fire ignited.
Three of the four workers injured were seriously burned, including a contractor. The refinery was completely shut down for just under two months and operated at reduced capacity for nearly a year.
KEY ISSUES:
• FREEZE PROTECTION OF DEAD-LEGS
• EMERGENCY ISOLATION OF EQUIPMENT
• FIREPROOFING OF SUPPORT STEEL
• FIRE PROTECTION FOR HIGH PRESSURE LPG SERVICE
• CHLORINE RELEASE
ROOT CAUSES:
1. The McKee Refinery had no formal written program in place to identify, review, and freeze-protect dead-legs or infrequently used piping and equipment, such as the propane mix control station.
2. The McKee Refinery did not apply Valero’s mandatory Emergency Isolation Valve procedure when evaluating risks in the PDA unit to ensure that the large quantities of flammable materials in the unit could be rapidly isolated in an emergency.
3. API guidance and Valero’s corporate Fire Proofing Specifications standard do not specify sufficiently protective distances for fireproofing pipe rack support steel for processes handling high-pressure flammables, such as the LPG in the PDA unit.
Image credit: CSB

Summary
An explosion at this 70,000 bbl-per-day oil refinery caused damage to the FCC, utilities, storage tanks, and asphalt unit. One employee was hospitalized for burns. Another person was injured when
Summary
An explosion at this 70,000 bbl-per-day oil refinery caused damage to the FCC, utilities, storage tanks, and asphalt unit. One employee was hospitalized for burns. Another person was injured when her car was struck by debris from the explosion on the nearby highway. There was a total of four injuries. A skeleton crew of just 40 people were on site because the blast occurred on a public holiday. There would typically have been about four times as many people on duty at the time of the explosion. The fire was brought under control the same day by the site’s fire brigade, supported by local fire departments. The release is believed to have occurred during a start-up on the propylene splitter unit, as a result of the catastrophic failure of a pump. Some processing resumed about two months later, and the FCC was re-commissioned eight months after the incident.
[ Property Damage $380 Million. Estimated Current Value $454 Million ]
Image credit: Delek
Summary
On Wednesday, February 18, 2015, an explosion occurred in the ExxonMobil Torrance, California refinery’s Electrostatic Precipitator (ESP), a pollution control device in the fluid catalytic cracking (FCC) unit that removes
Summary
On Wednesday, February 18, 2015, an explosion occurred in the ExxonMobil Torrance, California refinery’s Electrostatic Precipitator (ESP), a pollution control device in the fluid catalytic cracking (FCC) unit that removes catalyst particles using charged plates that produce sparks (potential ignition sources) during normal operation. The incident occurred when ExxonMobil was attempting to isolate equipment for maintenance while the unit was in an idled mode of operation; preparations for the maintenance activity caused a pressure deviation that allowed hydrocarbons to backflow through the process and ignite in the ESP.
The CSB found that this incident occurred due to weaknesses in the ExxonMobil Torrance refinery’s process safety management system. These weaknesses led to operation of the FCC unit without pre-established safe operating limits and criteria for unit shutdown, reliance on safeguards that could not be verified, the degradation of a safety-critical safeguard, and the re-use of a previous procedure deviation without a sufficient hazard analysis that confirmed that the assumed process conditions were still valid. .
KEY ISSUES:
• LACK OF SAFE OPERATING LIMITS & OPERATING PROCEDURE
• SAFEGUARD EFFECTIVENESS
• OPERATING EQUIPMENT BEYOND SAFE OPERATING LIFE
• RE-USE OF PREVIOUS PROCEDURE VARIANCE WITHOUT SUFFICIENT HAZARD ANALYSIS
ROOT CAUSES:
1. ExxonMobil did not establish the safe operating limits for operating the FCC unit in Safe Park (a standby mode of operation) or determine process conditions that required unit shutdown.
2. ExxonMobil did not perform a sufficient hazard analysis to determine if the unit conditions specified in the 2012 procedure were valid for the 2015 operation.
3. ExxonMobil operated FCC unit equipment beyond its predicted safe operating life.
4. ExxonMobil lacked safety instrumentation to detect flammable hydrocarbons flowing through the equipment and into the ESP.
5. ExxonMobil refinery management permitted opening process equipment without conforming to refinery standards.
Image credit: CSB

Summary
A February 20, 2003, dust explosion at the CTA Acoustics, Inc. (CTA) facility in Corbin, Kentucky, killed seven and injured 37 workers. This incident caused extensive damage to the production
Summary
A February 20, 2003, dust explosion at the CTA Acoustics, Inc. (CTA) facility in Corbin, Kentucky, killed seven and injured 37 workers. This incident caused extensive damage to the production area of the 302,000-square-foot plant. Nearby homes and an elementary school were evacuated, and a 12-mile section of Interstate 75 was closed. The largest CTA customer, Ford Motor Company, temporarily suspended operations at four automobile assembly plants because CTA had produced acoustic insulation products for those plants, as well as for other industrial and automotive clients.
KEY ISSUES:
• COMBUSTIBLE DUST HAZARD AWARENESS
• WORK PRACTICES
• BUILDING DESIGN
• PRODUCT STEWARDSHIP
ROOT CAUSES:
1. CTA management did not implement effective measures to prevent combustible dust explosions.
2. The CTA cleaning and maintenance procedures for production lines did not prevent the accumulation of unsafe levels of combustible dust on elevated flat surfaces.
3. The CTA incident investigation program did not ensure that all oven fires were investigated and that underlying causes were identified and resolved.
4. The Borden Chemical product stewardship program did not explicitly convey to CTA the explosive hazards of phenolic resins.
5. The original building design and subsequent building modifications did not effectively address the fire and explosion hazards associated with combustible dusts.
Image Credit: CSB

Summary
On February 23, 1999, a fire occurred in the crude unit at Tosco Corporation. Avon oil refinery in Martinez, California. Workers were attempting to replace piping attached to a 150-foot-tall
Summary
On February 23, 1999, a fire occurred in the crude unit at Tosco Corporation. Avon oil refinery in Martinez, California. Workers were attempting to replace piping attached to a 150-foot-tall fractionator tower while the process unit was in operation. During removal of the piping, naphtha was released onto the hot fractionator and ignited. The flames engulfed five workers located at different heights on the tower. Four men were killed, and one sustained serious injuries.
KEY ISSUES:
• CONTROL OF HAZARDOUS NONROUTINE MAINTENANCE
• MANAGEMENT OVERSIGHT & ACCOUNTABILITY
• MANAGEMENT OF CHANGE
• CORROSION CONTROL
ROOT CAUSES:
1. Tosco Avon refinery’s maintenance management system did not recognize or control serious hazards posed by performing nonroutine repair work while the crude processing unit remained in operation.
2. Tosco’s safety management oversight system did not detect or correct serious deficiencies in the execution of maintenance and review of process changes at its Avon refinery.
Image Credit: CSB

Summary
The earthquake struck with an intensity of M7.5 (MM IX), with aftershocks over the following weeks. The event caused building and infrastructure damage, and sinkholes and landslides. Over 160
Summary
The earthquake struck with an intensity of M7.5 (MM IX), with aftershocks over the following weeks. The event caused building and infrastructure damage, and sinkholes and landslides. Over 160 people were killed from the local communities and many injured.
The damage affected the local airport at Komo, which was significantly damaged, the gas conditioning plant — which was safely shut down with some damage but no loss of containment — and the pipeline system, where there was no loss of containment but a need to remediate the pipeline “right of way” along most of its onshore length.
March
Summary
The Rimbey pipeline system in Alberta, Canada transports liquid propane, butane and condensate products in an 8-inch pipeline. On the day of the incident the operating pumps were pumping against
Summary
The Rimbey pipeline system in Alberta, Canada transports liquid propane, butane and condensate products in an 8-inch pipeline. On the day of the incident the operating pumps were pumping against a closed valve. The line failed at a pressure of approximately 8000 kPa, which is below the 8372 kPa maximum operating pressure for the pipeline.
Liquid propane erupted violently and formed a pond of boiling propane. The propane quickly formed a ground level flammable gas cloud, which rolled across topsoil until it reached a road where it was ignited by a passing truck. Liquid propane entered a nearby storm sewer catchment basin. The propane spread into adjacent sewer lines. Explosive mixtures were detected over a wide area within the sewer system.
No injuries were recorded, however the incident instigated a large-scale evacuation of 19,000 people while efforts were made to eliminate the explosive danger.
A combination of water flushing, ventilation and nitrogen gas blanketing successfully eliminated the danger about 23 hours after the original fracture. Maintenance crews plugged the pipeline either side of the fracture to stop the flow of leaking gas
KEY ISSUES:
• EMERGENCY RESPONSE / SPILL CONTROL
Image Credit: Provincial Archives Of Alberta
Summary
A high-pressure steam (3.7 MPa) discharge occurred during a maintenance process, resulting in three field workers burned to death. Proximate causes: • Lack of work rules/policies/ standards/procedures (wrong procedures for inspections);
Summary
A high-pressure steam (3.7 MPa) discharge occurred during a maintenance process, resulting in three field workers burned to death.
Proximate causes:
• Lack of work rules/policies/ standards/procedures (wrong procedures for inspections);
• Inadequate work rules plan (lack of the pre-start safety review before inspection).
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
At approximately 6:15 p.m. on March 4, 1998, a catastrophic vessel failure and fire occurred near Pitkin, Louisiana, at the Temple 22-1 Common Point Separation Facility owned by Sonat Exploration
Summary
At approximately 6:15 p.m. on March 4, 1998, a catastrophic vessel failure and fire occurred near Pitkin, Louisiana, at the Temple 22-1 Common Point Separation Facility owned by Sonat Exploration Co. Four workers who were near the vessel were killed, and the facility sustained significant damage.
The facility housed two petroleum separation trains and consisted of separation equipment, piping, storage vessels, and a gas distribution system. The separation trains were designed to produce crude oil and natural gas from well fluid, derived from two nearby wells. The vessel ruptured due to overpressurization, releasing flammable material which then ignited.
KEY ISSUES:
• DESIGN & HAZARD REVIEWS
• PRESSURE-RELIEF DEVICES
• OPERATING PROCEDURES
ROOT CAUSES:
1. Sonat management did not use a formal engineering design review process or require effective hazard analyses in the course of designing and building the facility.
2. Sonat engineering specifications did not ensure that equipment that could potentially be exposed to high-pressure hazards was adequately protected by pressure-relief devices.
Image Credit: CSB

Summary
Some 25 miles of Trans-Andean pipeline disappeared in this event, which also damaged natural gas and gasoline pipelines. All 285 producing wells were shut down and oil exports were suspended
Summary
Some 25 miles of Trans-Andean pipeline disappeared in this event, which also damaged natural gas and gasoline pipelines. All 285 producing wells were shut down and oil exports were suspended and swap arrangement made with Venezuelan suppliers. The first earthquake registered 6.0 on the Richter scale, the second 6.8, and there was a total of 10 earthquakes in total. Repairs took several months.
[ Property Damage $120 Million. Estimated Current Value $288 Million ]
Image credit: NAPU
Summary
A hairline crack in a welded seam of piping to the level indicator system on an aldehyde column resulted in a minor ethylene oxide leak on this gas processing plant.
Summary
A hairline crack in a welded seam of piping to the level indicator system on an aldehyde column resulted in a minor ethylene oxide leak on this gas processing plant. As a result of this crack, which was caused by low cycle fatigue, ethylene oxide escaped near the level indicator and formed polyethylene glycols (PEG) in the mineral wool insulation. It is believed that both the leak and accumulation of PEG occurred over a period of time. During repairs to the level indicator, the metal sheathing of the insulation was removed and air contacted the insulation soaked with PEG. Auto-oxidation of the PEG resulted and the insulating material was ignited. The piping to the level indicator system was heated to such a degree that auto-decomposition of the ethylene oxide within the piping occurred. This autodecomposition propagated into the aldehyde column which subsequently exploded. The force of the explosion completely destroyed the distillation section of this plant. The large resulting fire and impact of flying debris to other process sections resulted in extensive damage throughout the plant.
[ Property Damage $79 Million. Estimated Current Value $178 Million ]
Image credit: No credit
Summary
A gas leak involving the pipe rack that runs to the terminal of this petrochemical complex led to an explosion, which occurred near the complex chemical plant, causing additional damage
Summary
A gas leak involving the pipe rack that runs to the terminal of this petrochemical complex led to an explosion, which occurred near the complex chemical plant, causing additional damage to the pipe rack and resulting in a major gas leak. A powerful second explosion occurred that could be felt more than 15 miles from the complex. These explosions and a subsequent fire completely destroyed the chemical plant, caused significant damage to the pipe rack, and resulted in moderate damage to other complex buildings and adjacent third-party facilities. The fire was extinguished after approximately three hours. Because of this incident, the chemical plant at this complex was completely shut down for seven months to allow for the rebuild of the plant and the pipe rack.
[ Property Damage $97 Million. Estimated Current Value $208 Million ]
Image credit: Reuters
Summary
A fire broke out in a wet gas scrubber while heavy maintenance on a unit was being carried out. Personnel were evacuated from the site and there were no injuries.
Summary
A fire broke out in a wet gas scrubber while heavy maintenance on a unit was being carried out. Personnel were evacuated from the site and there were no injuries. The site was conducting a planned shutdown and maintenance of the plant equipment including the polypropylene plant.
[ Property Damage $150 Million. Estimated Current Value $162 Million ]
Image credit: ORPIC
Summary
A major explosion occurred at a 145,000-barrels-per-day refinery in the north-eastern city of Sendai, hours after the largest earthquake in the country’s history was followed by a tsunami. The fire
Summary
A major explosion occurred at a 145,000-barrels-per-day refinery in the north-eastern city of Sendai, hours after the largest earthquake in the country’s history was followed by a tsunami. The fire at the Sendai refinery originated from a land oil product shipping facility. Workers at the refinery were evacuated, and there was no capacity available to extinguish the fire. Fire in the storage and shipping facilities had also damaged a 35,500 barrels-per-day FCC at the refinery.
[ Property Damage $590 Million. Estimated Current Value $651 Million ]
Image credit: JXTG Nippon Oil & Energy
Summary
An explosion occurred in the ethylene oxide process unit at this plant. As a result, the ethylene oxide refining column was completely destroyed, the ethylene glycol unit was substantially damaged,
Summary
An explosion occurred in the ethylene oxide process unit at this plant. As a result, the ethylene oxide refining column was completely destroyed, the ethylene glycol unit was substantially damaged, and the co-generation unit was partially damaged. A pipe rack near the storage area for liquid ethylene oxide was damaged when a large piece of shrapnel from the explosion hit the rack, rupturing lines which contained methane and other hydrocarbon products.
The subsequent fire that resulted from the released products was the only significant fire to occur during this incident. As a result of the explosion, all utilities at the plant were lost for approximately one week. Additionally, several fixed fire protection systems were damaged by the explosion or inadvertently actuated due to a loss of plant air. These systems were shut off, isolated, or placed back in service, as appropriate. A manual fire fighting effort was used to extinguish the fire in the pipe rack once the lines in the rack were isolated. The polyethylene production was restarted in early April 1991 using imported ethylene. The olefins production unit was restarted in late April 1991.
[ Property Damage $90 Million. Estimated Current Value $194 Million ]
Image credit: Vitaly Shmatikov
Summary
Fifteen months before the incident occurred it had been noticed that the flare line isolation valve V17 was passing. It was decided however to wait for a scheduled shutdown of
Summary
Fifteen months before the incident occurred it had been noticed that the flare line isolation valve V17 was passing. It was decided however to wait for a scheduled shutdown of the catalytic cracker unit and No 1 flare before commencing work on the valve. Gases from the remaining operating units were re-routed to No 2 and No 3 flares. This flare arrangement would allow the pipelines at V17 to be isolated.
When senior refinery staff prepared a plan for the isolation of the flare system, they concentrated on the operational and safety requirements of the flare system, making sure that no operational areas of the plant were inadvertently isolated. The details of the removal of V17 were not considered and left to those who would be responsible for the work.
Four workers were involved with the removal of the valve. When the majority of the bolts were undone the joint opened slightly and liquid dripped from a small gap between the flanges. The workers sought advice. The valve was checked and it was concluded that it was safe to carry on. Non ferrous hammers were provided before continuing with the removal. All the bolts were removed and the crane took the weight of a spacer and started to remove it, at which point gallons of liquid poured from the valve. A flammable vapour cloud formed from the rapidly spreading pool. The cloud reached the nearby air compressor, ignited and flashed back around the working area.
Two workers managed to escape the fire but a fitter and a rigger were engulfed by the flames and killed. The fire was allowed to burn in a controlled manner for almost two days while the rest of the refinery was shut down and the flare system purged with nitrogen
KEY ISSUES:
• DESIGN CODES – PIPEWORK
• MAINTENANCE PROCEDURES
• ISOLATION
Report: https://www.icheme.org/media/13700/the-fires-and-explosion-at-bp-oil-grangemouth-refinery-ltd.pdf
Image Credit: HSE
Summary
A fire occurred on one of the two hydrotreaters on an oil sands upgrader facility. The fire was reported to be as a result of the failure of a pipe,
Summary
A fire occurred on one of the two hydrotreaters on an oil sands upgrader facility. The fire was reported to be as a result of the failure of a pipe, resulting in a releaser of naphtha. One worker was seriously injured as a result of the fire, which was extinguished after two days.
[ Property Damage $220 Million. Estimated Current Value $220 Million ]
Image credit: CBC
Summary
The world’s largest offshore production facility was rocked by a series of explosions caused by a gas release. The explosions knocked out a support pillar of the semi-submersible platform allowing
Summary
The world’s largest offshore production facility was rocked by a series of explosions caused by a gas release. The explosions knocked out a support pillar of the semi-submersible platform allowing seawater to enter the vessel. Workers pumped in nitrogen and compressed air and tried to pump out almost 3,000 metric tons of seawater to keep the rig afloat, but were unsuccessful. On March 20, 2001, the rig sank to the sea floor. The incident killed 11 workers.
[ Property Damage $500 Million. Estimated Current Value $851 Million ]
Ref: http://www.anp.gov.br/noticias/2342-anp-marinha-comissao-conjunta
Image credit: Petrobras
Related Events
Summary
On Sunday, March 17, 2019, at approximately 10:00 am, a large fire erupted at the Intercontinental Terminals Company, LLC (ITC) bulk liquid storage terminal located in Deer Park, Texas (Figure
Summary
On Sunday, March 17, 2019, at approximately 10:00 am, a large fire erupted at the Intercontinental Terminals Company, LLC (ITC) bulk liquid storage terminal located in Deer Park, Texas (Figure 1). The fire originated in the vicinity of Tank 80-8, an 80,000-barrel aboveground atmospheric storage tank that held naphtha, a flammable liquid, typically used as a feedstock or blend stock for production of gasoline. ITC was unable to isolate or stop the release of naphtha product from the tank, and the fire continued to burn, intensify, and progressively involved additional tanks in the tank farm. The fire was extinguished on the morning of March 20, 2019.
The incident did not result in any injuries to either ITC personnel or emergency responders. However, the local community experienced disruptions, including several shelter-in-place notifications, which prompted local schools and businesses either to close or operate under modified conditions.
KEY ISSUES:
• RELEASE DETECTION
• RELEASE ISOLATION
• PROLONGED EMERGENCY RESPONSE
Image credit: CSB

Summary
Contract personnel were installing a pig trap on an 18-inch-diameter export gas pipeline on the platform. As a cold cut was made into the pipeline, hydrocarbons sprayed from the cut
Summary
Contract personnel were installing a pig trap on an 18-inch-diameter export gas pipeline on the platform. As a cold cut was made into the pipeline, hydrocarbons sprayed from the cut and ignited. The explosion and fire burned the main structure and caused subsequent explosions when six other pipelines ruptured due to the intense heat. The accident resulted in the total destruction of the platform and seven fatalities. It took two years to replace the platform.
[ Property Damage $400 Million. Estimated Current Value $899 Million ]
Image credit: ARCO
Summary
On 20 March 1990 the halogen exchange reactor on the Fluoroaromatics plant was ruptured by the pressure generated by a runaway reaction. The plant was partially destroyed and missiles were
Summary
On 20 March 1990 the halogen exchange reactor on the Fluoroaromatics plant was ruptured by the pressure generated by a runaway reaction. The plant was partially destroyed and missiles were projected over 500m. Six employees were injured and one subsequently died from post-operative complications.
A batch had been charged into the vessel and was being heated up as normal. When it reached 165oC, the temperature continued to rise and the operators adjusted the jacket temperature. The display screen in use did not display pressure and they were unaware of a corresponding rise in pressure. By the time they were alerted to the rise in pressure the pressure relief valves had lifted. Before any other corrective action could be taken, the reactor exploded. The pressure in the vessel reached a value of about 60-80 barg compared with the relief valve set pressure of 5 barg.
The resulting blast was enhanced by the formation of a fireball, which occurred when the contents of the reactor ignited within the plant structure. This started local fires and initiated what became a major conflagration in an adjacent unit where vessels containing xylene were damaged by the blast/missile effects. The ensuing fires were brought under control in four hours by the Shell fire team and Cheshire fire service.
The initial cause of the incident was the ingress of excessive water into the process leading to the formation of acetic acid which, upon recycle to the reactor, reacted vigorously with the reactor contents initiating the explosion. Water was present as a part of the process, however a massive incursion led to the formation of a separate layer in the process vessel which was not removed but recycled back into reactor.
KEY ISSUES:
• CONTROL ROOM DESIGN
• RAW MATERIALS CONTROL / SAMPLING
• REACTION / PRODUCT TESTING
• RELIEF SYSTEMS / VENT SYSTEMS
Image Credit: The Leader
Summary
An accident occurred at a methylcellulose manufacturing facility. An explosion occurred and was followed by a fire, which was extinguished about seven hours later. A total of 17 people working
Summary
An accident occurred at a methylcellulose manufacturing facility. An explosion occurred and was followed by a fire, which was extinguished about seven hours later. A total of 17 people working at the site were injured in this accident; three critically, five seriously, and nine with minor injuries. There was one minor injury off site. Ignition of the methylcellulose powder is though to have been due to static electricity, resulting in a powder dust explosion. All methylcellulose operations were suspended for two months before sequentially restarting.
[ Property Damage $240 Million. Estimated Current Value $306 Million ]
Image credit: Shin-Etsu
Summary
On Saturday 21 March 1987 the hydrocracker unit was being recommissioned following a routine shut down. During the recommissioning a plant trip occurred. This was thought to be a spurious
Summary
On Saturday 21 March 1987 the hydrocracker unit was being recommissioned following a routine shut down. During the recommissioning a plant trip occurred. This was thought to be a spurious trip and the plant operators started to bring up the unit to normal operating conditions. From then on until the time of the incident the plant was held in stand by condition with no fresh feed.
At 07:00 hours the following morning there was a violent explosion and subsequent fire. The explosion could be heard and felt up to 30km away. The explosion centred on a low pressure (LP) separator vessel, V306, which was fabricated from 18mm steel plate and weighed 20 tonnes.
The investigation of the accident suggested that an air operated control valve on the high pressure (HP) separator had been opened and closed on manual control at least three times. Liquid level in the LP separator fell and the valve was opened. This action allowed the remaining liquid in the HP separator to drain away and for high pressure gas to break through into the LP separator. As the pressure relief on the LP separator had been designed for a fire relief case, not gas breakthrough the vessel subsequently exploded.
The control valve did not close automatically because the low low level trip on the HP separator had been disconnected several years earlier. The operators did not trust the main level control reading and referred to a chart recorder for a back up level reading. There was an offset on this chart recorder which led them to assume that the level in the HP separator was normal.
KEY ISSUES:
• MAINTENANCE PROCEDURES
• CONTROL SYSTEMS
• OPERATING PROCEDURES
• PLANT MODIFICATION / CHANGE PROCEDURES
• ALARM / TRIPS / INTERLOCKS
• RELIEF SYSTEMS / VENT SYSTEMS
• ISOLATION
Report: https://www.icheme.org/media/13700/the-fires-and-explosion-at-bp-oil-grangemouth-refinery-ltd.pdf
Image Credit: HSE
Summary
At approximately 1:20 p.m. on March 23, 2005, a series of explosions occurred at the BP Texas City refinery during the restarting of a hydrocarbon isomerization unit. Fifteen workers were
Summary
At approximately 1:20 p.m. on March 23, 2005, a series of explosions occurred at the BP Texas City refinery during the restarting of a hydrocarbon isomerization unit. Fifteen workers were killed and 180 others were injured. Many of the victims were in or around work trailers located near an atmospheric vent stack. The explosions occurred when a distillation tower flooded with hydrocarbons and was overpressurized, causing a geyser-like release from the vent stack.
KEY ISSUES:
• SAFETY CULTURE
• REGULATORY OVERSIGHT
• PROCESS SAFETY METRICS
• HUMAN FACTORS
ROOT CAUSES:
1. BP Group Board did not provide effective oversight of the company’s safety culture and major accident prevention programs.
2. Senior executives:
• inadequately addressed controlling major hazard risk. Personal safety was measured, rewarded, and the primary focus, but the same emphasis was not put on improving process safety performance;
• did not provide effective safety culture leadership and oversight to prevent catastrophic accidents;
• ineffectively ensured that the safety implications of major organizational, personnel, and policy changes were evaluated;
• did not provide adequate resources to prevent major accidents; budget cuts impaired process safety performance at the Texas City refinery.
3. BP Texas City Managers did not:
• create an effective reporting and learning culture; reporting bad news was not encouraged. Incidents were often ineffectively investigated and appropriate corrective actions not taken.
• ensure that supervisors and management modeled and enforced use of up-to-date plant policies and procedures.
• incorporate good practice design in the operation of the ISOM unit.
• ensure that operators were supervised and supported by experienced, technically trained personnel during unit startup, an especially hazardous phase of operation; or that
• effectively incorporated human factor considerations in its training, staffing, and work schedule for operations personnel.
Image Credit: CSB

Related Events
Topics
Summary
On March 24, 1989, shortly after midnight, the oil tanker Exxon Valdez struck Bligh Reef in Prince William Sound, Alaska, spilling more than 11 million gallons of crude oil. The
Summary
On March 24, 1989, shortly after midnight, the oil tanker Exxon Valdez struck Bligh Reef in Prince William Sound, Alaska, spilling more than 11 million gallons of crude oil. The spill was the largest in U.S. history and tested the abilities of local, national, and industrial organizations to prepare for, and respond to, a disaster of such magnitude. Many factors complicated the cleanup efforts following the spill. The size of the spill and its remote location, accessible only by helicopter and boat, made government and industry efforts difficult and tested existing plans for dealing with such an event.
The spill posed threats to the delicate food chain that supports Prince William Sound’s commercial fishing industry. Also in danger were ten million migratory shore birds and waterfowl, hundreds of sea otters, dozens of other species, such as harbor porpoises and sea lions, and several varieties of whales.
Image Credit: EPA
Related Events
Summary
An apparent failure of a propane intercooler liquid level control during unsupervised maintenance led to an explosion and fire. The control room on the main platform was destroyed and adjacent
Summary
An apparent failure of a propane intercooler liquid level control during unsupervised maintenance led to an explosion and fire. The control room on the main platform was destroyed and adjacent platforms were affected by the blast wave. There were 11 fatalities.
[ Property Damage $100 Million. Estimated Current Value $194 Million ]
Image credit: PDVSA
Summary
This explosion was caused by the failure of a valve bonnet in a high-pressure section of a 60,000 bbl-per-day hydrocracker. A vapor cloud formed from the release, ignited, and was
Summary
This explosion was caused by the failure of a valve bonnet in a high-pressure section of a 60,000 bbl-per-day hydrocracker. A vapor cloud formed from the release, ignited, and was followed by a large fire fed by escaping hydrocarbons at high pressure. The explosion resulted in the collapse of a large section of pipe rack and destruction of a large fin-fan cooler mounted above the rack. Many pumps were destroyed and a separator was badly damaged. Approximately 300 fire fighters and 33 fire trucks participated in the two and a half-hour effort to control the fire. Foam concentrate consumed totalled 3,200 US gallons. The hydrocracker was out of service for 12 months.
[ Property Damage $113 Million. Estimated Current Value $205 Million ]
Image credit: SF Gate
Summary
Blaze in a warehouse next to oil factory. Fire created massive plumes of smoke in the area. Fire spread to adjacent paint factory. Damaged buildings Source: A web-based collection and
Summary
Blaze in a warehouse next to oil factory. Fire created massive plumes of smoke in the area. Fire spread to adjacent paint factory. Damaged buildings
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: Twitter / News24
April
Summary
A complex of six platforms located in 30 meters of water in the Gulf of Mexico was subject to a major fire. The fire originated on the lower decks of
Summary
A complex of six platforms located in 30 meters of water in the Gulf of Mexico was subject to a major fire. The fire originated on the lower decks of the production platform and resulted in major damage to that platform, radiation and fire damage to an adjacent compression platform, the loss of bridge links and pipelines, and radiation damage to other bridge links. The root-cause investigation required by the government identified corrosion of a small bore pipeline as the cause of the initial failure.
[ Property Damage $500 Million. Estimated Current Value $650 Million ]
Image credit: PEMEX
Summary
A fire started inside a depot with 3 million liters of diesel and the flames spread to four neighboring storage tanks. The fire lasted for 9 days. Fine of around USD
Summary
A fire started inside a depot with 3 million liters of diesel and the flames spread to four neighboring storage tanks. The fire lasted for 9 days.
Fine of around USD $6.4 million (R$ 22.5 million). Environmental impact causing death of thousands of fish
Proximate causes:
• Inadequate management/ supervision
• Inadequate work planning
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: Paulo Whitaker / Reuters
Summary
A fire broke out in the 188,000 barrels-per-day refinery, caused by flash-floods during heavy rain. The rain overwhelmed the storm drainage system on the refinery, resulting in hydrocarbons being washed
Summary
A fire broke out in the 188,000 barrels-per-day refinery, caused by flash-floods during heavy rain. The rain overwhelmed the storm drainage system on the refinery, resulting in hydrocarbons being washed out of the drains and around the site. An explosion was reported in the crude distillation unit. There were two fires in the crude distillation unit (CDU), one in the coking plant and two in the topping distillation plant. The government agency said the incident had been caused by hydrocarbons exploding in one of the coke manufacturing furnaces. The furnaces had been shut down, but were still hot enough to ignite the hydrocarbon. It took eight hours to extinguish the fire and 10 hours before the incident was under control. There were no fatalities or injuries.
[ Property Damage $225 Million. Estimated Current Value $243 Million ]
Image credit: YPF
Summary
On April 2, 2010, the Tesoro Refining and Marketing Company LLC (‘Tesoro’) petroleum refinery in Anacortes, Washington (‘the Tesoro Anacortes Refinery’), experienced a catastrophic rupture of a heat exchanger in
Summary
On April 2, 2010, the Tesoro Refining and Marketing Company LLC (‘Tesoro’) petroleum refinery in Anacortes, Washington (‘the Tesoro Anacortes Refinery’), experienced a catastrophic rupture of a heat exchanger in the Catalytic Reformer / Naphtha Hydrotreater unit (‘the NHT unit’). The heat exchanger, known as E-6600E (‘the E heat exchanger’), catastrophically ruptured because of High Temperature Hydrogen Attack (HTHA). Highly flammable hydrogen and naphtha at more than 500 degrees Fahrenheit (°F) were released from the ruptured heat exchanger and ignited, causing an explosion and an intense fire that burned for more than three hours. The rupture fatally injured seven Tesoro employees (one shift supervisor and six operators) who were working in the immediate vicinity of the heat exchanger at the time of the incident. To date this is the largest fatal incident at a US petroleum refinery since the BP Texas City accident in March 2005.
The NHT unit at the Tesoro Anacortes Refinery contained two parallel groups, or banks, of three heat exchangers (A/B/C and D/E/F) used to preheat process fluid before it entered a reactor, where impurities were treated for subsequent removal. The E heat exchanger was constructed of carbon steel.
At the time of the release, the Tesoro workers were in the final stages of a startup activity to put the A/B/C bank of heat exchangers back in service following cleaning. The D/E/F heat exchangers remained in service during this operation. Because of the refinery’s long history of frequent leaks and occasional fires during this startup activity, the CSB considers this work to be hazardous and nonroutine. While the operations staff was performing the startup operations, the E heat exchanger in the middle of the operating D/E/F bank catastrophically ruptured. .
KEY ISSUES:
• INHERENTLY SAFER DESIGN
• TESORO PROCESS SAFETY CULTURE
• CONTROL OF NONROUTINE WORK
• MECHANICAL INTEGRITY INDUSTRY STANDARD DEFICIENCIES
• REGULATORY OVERSIGHT OF PETROLEUM REFINERIES
ROOT CAUSES:
1. High Temperature Hydrogen Attack
2. NHT Heat Exchanger Flanges – A History of Leaking
3. Hazardous Nonroutine Work
4. Process Hazard Analyses Failed to Prevent or Reduce the Consequences
Image credit: CSB

Summary
On Tuesday, April 2, 2019, just before 10:46 am, a vapor cloud of isobutylene formed at the KMCO, LLC (‘KMCO’) facility in Crosby, Texas after a three-inch gray iron (a
Summary
On Tuesday, April 2, 2019, just before 10:46 am, a vapor cloud of isobutylene formed at the KMCO, LLC (‘KMCO’) facility in Crosby, Texas after a three-inch gray iron (a type of cast iron) y-strainer, a piping component, failed.
Shortly after 10:50 am, the vapor cloud found an ignition source and ignited, causing an explosion. The explosion killed one KMCO worker and seriously burned two others. On the day of the incident, more than 200 KMCO employees, contract workers, and visitors were onsite. The incident injured at least 30 workers (seven KMCO employees and 23 contract workers). A shelter-in-place was issued to community members within one mile of the KMCO facility.
KEY ISSUES:
• MECHANICAL INTEGRITY
Image credit: CSB

Summary
A blast occurred in a pumping station, after leaking oil caught fire. 177 fire engines and more than 800 firefighters were rushed to the blaze, and more than 14,000 residents
Summary
A blast occurred in a pumping station, after leaking oil caught fire. 177 fire engines and more than 800 firefighters were rushed to the blaze, and more than 14,000 residents in the surrounding area were evacuated.
Proximate causes:
• Improper use of protective methods (Improper welding of conveying pipe)
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: Getty
Summary
On April 7, 2003, at about 8:55 p.m., central daylight time, an 80,000-barrel storage tank at ConocoPhillips Company’s Glenpool South tank farm in Glenpool, Oklahoma, exploded and burned as it
Summary
On April 7, 2003, at about 8:55 p.m., central daylight time, an 80,000-barrel storage tank at ConocoPhillips Company’s Glenpool South tank farm in Glenpool, Oklahoma, exploded and burned as it was being filled with diesel. The tank, designated tank 11, had previously contained gasoline, which had been removed from the tank earlier in the day. The tank contained between 7,397 and 7,600 barrels of diesel at the time of the explosion.
The resulting fire burned for about 21 hours and damaged two other storage tanks in the area. The cost of the accident, including emergency response, environmental remediation, evacuation, lost product, property damage, and claims, was $2,357,483. There were no injuries or fatalities. Nearby residents were evacuated, and schools were closed for 2 days.
Image Credit: NTSB
Summary
On April 8, 2004, four workers were seriously injured when highly flammable gasoline components were released and ignited at the Giant Industries Ciniza refinery, east of Gallup, New Mexico. The
Summary
On April 8, 2004, four workers were seriously injured when highly flammable gasoline components were released and ignited at the Giant Industries Ciniza refinery, east of Gallup, New Mexico. The release occurred as maintenance workers were removing a malfunctioning pump from the refinery’s hydrofluoric acid (HF) alkylation unit. Unknown to personnel, a shut-off valve connecting the pump to a distillation column was apparently in the open position, leading to the release and subsequent explosions.
KEY ISSUES:
• MECHANICAL INTEGRITY
• CORROSION & SCALE FORMATION
• VALVE DESIGN
• HUMAN FACTORS CONSIDERATION
• MANAGEMENT OF CHANGE
• LOCKOUT/TAGOUT & ISOLATION
ROOT CAUSES:
1. An MOC hazard analysis was not conducted.
2. the facility lacked procedures to verify that the pump had been isolated, depressurized and drained.
3. Instead of determining the cause of frequent pump malfunctions and then implementing a program that would prevent problems before they occurred, Giant used breakdown maintenance by making repeated repairs to the pump seals after failure.
Image Credit: CSB

Summary
Two employees accidently fell in an aerobic tank sewage treatment station. Two more employees fell into the aerobic tank in the subsequent rescue. Proximate causes: • Inadequate tools, equipment & vehicles
Summary
Two employees accidently fell in an aerobic tank sewage treatment station. Two more employees fell into the aerobic tank in the subsequent rescue.
Proximate causes:
• Inadequate tools, equipment & vehicles (Aerobic tank no special ventilation equipment)
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
An oil spill occurred due to a failure of a block valve to seat properly during maintenance on a pump strainer in the visbreaker unit. The oil auto-ignited and the
Summary
An oil spill occurred due to a failure of a block valve to seat properly during maintenance on a pump strainer in the visbreaker unit. The oil auto-ignited and the ensuing fire spread and destroyed the visbreaker and damaged adjacent equipment. Subsequent explosions, heat restricted fire fighting access, inadequately trained fire brigade personnel, and damage to the firewater distribution system further hindered extinguishing the fire in a timely manner. The fire was spread by the firewater application, and was finally extinguished with the help of the local fire department.
[ Property Damage $159 Million. Estimated Current Value $271 Million ]
Image credit: Citgo
Summary
On April 9, 1998, an 18,000-gallon propane tank exploded at the Herrig Brothers farm in Albert City, Iowa. The explosion killed two volunteer firefighters and injured seven other emergency response
Summary
On April 9, 1998, an 18,000-gallon propane tank exploded at the Herrig Brothers farm in Albert City, Iowa. The explosion killed two volunteer firefighters and injured seven other emergency response personnel. Several buildings were also damaged by the blast.
KEY ISSUES:
• DESIGN & INSTALLATION DEFICIENCIES
• REGULATORY OVERSIGHT
• BLEVE HAZARD & EMERGENCY RESPONSE
ROOT CAUSES:
1. Protection for aboveground piping was inadequate.
2. The diameter of the pipe downstream from an excess flow valve was too narrow, which prevented the valve from functioning properly.
3. Fire fighter training for responding to BLEVEs was inadequate.
Image Credit: CSB

Related Events
Summary
A crack occurred in a pipeline (diameter 200 mm) conveying oil and gas, and the following fire damaged three pumps and some instrumentation Proximate causes: • Inadequate tools, equipment & vehicles
Summary
A crack occurred in a pipeline (diameter 200 mm) conveying oil and gas, and the following fire damaged three pumps and some instrumentation
Proximate causes:
• Inadequate tools, equipment & vehicles (Equipment failure: sealing failure and pipe leak)
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
A two-inch-diameter line carrying hydrogen gas at 3,000 psi failed at a weld, resulting in a high pressure hydrogen fire. The fire resulted in flame impingement on the calcium silicate
Summary
A two-inch-diameter line carrying hydrogen gas at 3,000 psi failed at a weld, resulting in a high pressure hydrogen fire. The fire resulted in flame impingement on the calcium silicate insulation of the skirt for a 100-feet-high reactor in a hydrocracker unit. The steel skirt for this reactor, which was between 10 and 12 feet in diameter and had a wall thickness of seven inches, subsequently failed. The falling reactor damaged air coolers and other process equipment, greatly increasing the size of the loss. At the time of the incident, the hydrocracker unit was being shut down for maintenance and the reactor was in a hydrogen purge cycle. The initial hydrogen leak is believed to have resulted from the failure of an elbow to reducer weld in the two-inch-diameter hydrogen preheat exchanger by-pass line.
[ Property Damage $90 Million. Estimated Current Value $202 Million ]
Image credit: San Francisco Chronicle
Summary
On the night of April 12, 2004, during an attempt to make the first production batch of triallyl cyanurate (TAC) at MFG Chemical, Inc. (MFG) in Dalton, Georgia, a runaway
Summary
On the night of April 12, 2004, during an attempt to make the first production batch of triallyl cyanurate (TAC) at MFG Chemical, Inc. (MFG) in Dalton, Georgia, a runaway chemical reaction released highly toxic and flammable allyl alcohol and toxic allyl chloride into the nearby community. The fire department ordered an evacuation of residents and businesses within a halfmile of the facility. The release forced more than 200 families from their homes. One MFG employee sustained minor chemical burns and 154 people received decontamination and treatment at the local hospital for chemical exposure, including 15 police and ambulance personnel assisting with the evacuation. Five residents required overnight hospitalization for breathing difficulties. The reactor continued venting toxic vapor for nearly eight hours and the evacuation order lasted more than nine hours.
KEY ISSUES:
• REACTIVE CHEMICALS PROCESS DESIGN
• PROCESS SCALE-UP
• EMERGENCY PLANNING & RESPONSE
ROOT CAUSES:
1. MFG did not understand or anticipate the reactive chemistry hazards. They did not make use of readily available literature on the hazards of reactive chemistry, or conduct a comprehensive literature search of the reactive chemistry specifically involved in manufacturing the product, which would have alerted them to the hazards involved in manufacturing TAC.
2. MFG did not perform a comprehensive process design and hazard review of the laboratory scale-up to full production before attempting the first production run.
3. MFG did not prepare and implement an adequate emergency response plan. They did not train or equip employees to conduct emergency mitigation actions.
4. MFG did not implement the EPA Risk Management Program or the OSHA Process Safety Management program prior to receiving the allyl alcohol. The regulations require comprehensive engineering analyses of the process, emergency planning, a pre-startup safety review, and coordination with the local community before receiving the covered chemical at the site and introducing the covered chemical into the process.
Image Credit: CSB

Related Events
Summary
A natural gas pipeline that was situated within a plowed field exploded and caused a fire. The location of the explosion helped crews keep it contained. One home was voluntarily
Summary
A natural gas pipeline that was situated within a plowed field exploded and caused a fire. The location of the explosion helped crews keep it contained. One home was voluntarily evacuated
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: News Channel 10 Amarillo
Summary
The incident took place on Easter Monday the 16th April 2001. During the morning the SGP was operating normally and the Central Control Room (CCR) reported a quiet shift, with
Summary
The incident took place on Easter Monday the 16th April 2001. During the morning the SGP was operating normally and the Central Control Room (CCR) reported a quiet shift, with no alarms showing for the SGP. In the early afternoon there were only 185 people on site, rather than a normal weekday figure of about 800. Most of the staff were inside buildings preparing for the shift handover, which was due to occur at 3pm. A number of people were working in the open air.
At approximately 14.20 hrs a catastrophic failure of a section of pipework on the SGP plant occurred at an elbow just downstream of a water-into-gas injection point. The six inch diameter pipe P4363, (the overhead line carrying flammable gas under high pressure),ruptured releasing a huge cloud containing around 90% ethane/propane/butane. About 20-30 seconds later the gas cloud ignited. As a result a massive explosion and fire followed.
KEY LESSONS:
Management of Pipework Inspection
• Effective pipework inspection systems are a vital major accident prevention measure for high hazard pipework.
• Such systems should at least meet current industry good practice standard.
• Decisions on inspection intervals should be informed by suitable and sufficient information on process conditions and previous inspection findings.
Management of Change
• Effective management of change systems, which consider both plant and process modifications, are essential to prevent major accidents.
• Particular care is needed to ensure that ‘quick fix’ modifications, during the commissioning and early operation phases of new plant, are covered.
Management of Corrosion
• Systematic and thorough arrangements are necessary for the effective management of corrosion on major hazard installations.
• Such arrangements should ensure that any available information on relevant corrosion degradation mechanisms is identified and acted on.
• Adequate resource, including relevant expertise, should be applied to ensure that adequate standards are achieved and maintained.
Communication
• Effective communication is an important element of any safety management system. In the context of major hazard establishments the accurate recording and effective sharing of information and data relevant to plant corrosion is essential for major accident prevention.
• Communication systems should aim to actively involve the workforce in the prevention of major accidents as part of an adequately resourced process safety management system.
Image Credit: HSE
Related Events
Summary
During the transfer of acetal from one vessel to another a fire and explosion occurred due a chemical reaction, which caused the rupture of one of the vessels. Source: A
Summary
During the transfer of acetal from one vessel to another a fire and explosion occurred due a chemical reaction, which caused the rupture of one of the vessels.
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: Unidentified
Summary
On April 20, 2010, a multiple-fatality incident occurred at the Macondo oil well approximately 50 miles off the coast of Louisiana in the Gulf of Mexico during temporary well-abandonment activities
Summary
On April 20, 2010, a multiple-fatality incident occurred at the Macondo oil well approximately 50 miles off the coast of Louisiana in the Gulf of Mexico during temporary well-abandonment activities on the Deepwater Horizon (DWH) drilling rig. Control of the well was lost, resulting in a blowout—the uncontrolled release of oil and gas (hydrocarbons) from the well. On the rig, the hydrocarbons found an ignition source and ignited. The resulting explosions and fire led to the deaths of 11 individuals, serious physical injuries to 17 others, the evacuation of 115 individuals from the rig, the sinking of the Deepwater Horizon, and massive marine and coastal damage from a reported 4 million barrels of released hydrocarbons.
BP was the main operator/lease holder responsible for the well design, and Transocean was the drilling contractor that owned and operated the DWH. On the day of the incident, the crew was completing temporary abandonment of the well so that it could be left in a safe condition until a production facility could return later to extract oil and gas from it.
Abandonment activities would essentially plug the well. Earlier, a critical cement barrier intended to keep the hydrocarbons below the seafloor had not been effectively installed at the bottom of the well. BP and Transocean personnel misinterpreted a test to assess cement barrier integrity, leading them to erroneously believe that the hydrocarbon bearing zone at the bottom of the well had been sealed. When the crew removed drilling mud from the well in preparation to install an additional cement barrier, the open blowout preventer (BOP) was the only physical barrier that could have potentially prevented hydrocarbons from reaching the rig and surrounding environment. The ability of the BOP to act as this barrier was contingent primarily upon human detection of the kick and timely activation and closure of the BOP.
Removing drilling mud after the test allowed hydrocarbons to flow past the failed cement barrier toward the DWH. The hydrocarbons continued to flow from the reservoir for almost an hour without human detection or the activation of the automated controls to close the BOP. Eventually, oil and gas passed above the BOP and forcefully released onto the rig. In response, the well operations crew manually closed the BOP. Oil and gas that had already flowed past the BOP continued to gush onto the rig, igniting and exploding. The explosion likely activated an automatic emergency response system designed to shear drillpipe passing through the BOP and seal the well, but it was unsuccessful.
KEY ISSUES:
• BOP TECHNICAL FAILURE ANALYSIS
• BARRIER MANAGEMENT AT MACONDO
• SAFETY CRITICAL ELEMENTS
• HUMAN FACTORS
• ORGANIZATIONAL LEARNING
• SAFETY PERFORMANCE INDICATORS
• RISK MANAGEMENT PRACTICES
• CORPORATE GOVERNANCE
• SAFETY CULTURE
ROOT CAUSES:
1. Technical Factors
2. Human and Organizational Factors
3. Regulatory Factors
Image Credit: CSB

Related Events
Summary
On April 23, 2004, an explosion and fire killed five and seriously injured three workers at the Formosa Plastics Corporation, IL (Formosa-IL) PVC manufacturing facility in Illiopolis, Illinois. The explosion
Summary
On April 23, 2004, an explosion and fire killed five and seriously injured three workers at the Formosa Plastics Corporation, IL (Formosa-IL) PVC manufacturing facility in Illiopolis, Illinois. The explosion occurred after a large quantity of highly flammable vinyl chloride monomer (VCM) was inadvertently released from a reactor and ignited. The explosion and fire that followed destroyed much of the facility and burned for two days. Local authorities ordered residents within one mile of the facility to evacuate.
KEY ISSUES:
• HUMAN FACTORS
• HAZARD EVALUATION
• INCIDENT INVESTIGATION
• EMERGENCY RESPONSE
ROOT CAUSES:
1. Borden Chemical did not adequately address the potential for human error.
2. Formosa-IL did not adequately address the potential for human error.
3. Formosa-IL relied on a written procedure to control a hazard with potentially catastrophic consequences.
Image Credit: CSB

Related Events
Summary
A piping leak resulted in a fire in this refinery coker unit. Smoke rose to over 3,000 feet, and the coker was shut down for approximately two months. [ Property
Summary
A piping leak resulted in a fire in this refinery coker unit. Smoke rose to over 3,000 feet, and the coker was shut down for approximately two months.
[ Property Damage $120 Million. Estimated Current Value $204 Million ]
Image credit: Tosco
Summary
During the conversion of one of the platform wells from oil to gas production, a high-pressure gas pocket was encountered that forced the drill pipe out of the well. The
Summary
During the conversion of one of the platform wells from oil to gas production, a high-pressure gas pocket was encountered that forced the drill pipe out of the well. The business operations platform (BOP) failed to shut in the well, and sparks, caused by the drill pipe that was ejected from the well hitting one of the platform legs, ignited the escaping gas. The fire lasted for 31 days. The majority of the topside structure was destroyed and the facility was later declared a total loss. Redesign of the production module was completed in 45 days in an effort to shorten the loss of production as much as possible. Full production was restored 18 months after the loss.
[ Property Damage $330 Million. Estimated Current Value $762 Million ]
Image credit: Petrobras
Summary
On April 26, 2018, an explosion and subsequent fire occurred at the Superior Refinery Company LLC refinery in Superior, Wisconsin (‘Husky Superior Refinery’). The incident occurred in the refinery’s Fluid
Summary
On April 26, 2018, an explosion and subsequent fire occurred at the Superior Refinery Company LLC refinery in Superior, Wisconsin (‘Husky Superior Refinery’). The incident occurred in the refinery’s Fluid Catalytic Cracking Unit (FCCU). In preparation for the shutdown, the refinery brought in hundreds of contractors and increased operations staffing. The contractors were performing many tasks such as electrical work, preparing for chemical cleaning, building scaffolding, and welding. As a result of the explosion, thirty-six people sought medical attention, including eleven refinery and contract workers who suffered OSHA recordable injuries. In addition, a large portion of Superior, Wisconsin was evacuated. The refinery was shutting down in preparation for a five-week turnaround when an explosion occurred, sending several people to area hospitals with injuries.
KEY ISSUES:
• PYROPHORIC IRON SULFIDE
Image credit: CSB

Summary
A shelter-in-place was ordered when a fire broke out following an explosion in the propylene refrigeration section of an ethylene unit. The fire, which burned for three days, forced the
Summary
A shelter-in-place was ordered when a fire broke out following an explosion in the propylene refrigeration section of an ethylene unit. The fire, which burned for three days, forced the shutdown of the facility for approximately six months, but caused no deaths or serious injuries.
[ Property Damage $200 Million. Estimated Current Value $268 Million ]
Image credit: Mark M. Hancock
Summary
Two firefighters were injured tackling a blaze at a refinery. The incident occurred when crude oil leaked from a pipe supplying the refinery from bulk storage tanks. [ Property Damage
Summary
Two firefighters were injured tackling a blaze at a refinery. The incident occurred when crude oil leaked from a pipe supplying the refinery from bulk storage tanks.
[ Property Damage $110 Million. Estimated Current Value $147 Million ]
Image credit: ISAB
May
Summary
Workers were preparing to check a compressor in the nitroparaffin unit when they noticed a small fire and sounded the plant fire alarm. About 30 seconds later, an explosion occurred,
Summary
Workers were preparing to check a compressor in the nitroparaffin unit when they noticed a small fire and sounded the plant fire alarm. About 30 seconds later, an explosion occurred, which was followed by a series of smaller explosions. The effects of the initial explosion were reported as far away as eight miles from the plant. Additionally, the initial explosion completely damaged an area of the plant approximately the size of a city block. Subsequent fires were reported to have burned for more than seven hours. Although the incident did not damage the two ammonia units on site, the entire plant was temporarily shut down for precautionary measures.
[ Property Damage $120 Million. Estimated Current Value $257 Million ]
Image credit: No credit
Summary
In the early morning hours of May 1, 2002, a fire erupted at the Third Coast Industries Friendswood facility, located in an unincorporated area of Brazoria County, Texas. The facility
Summary
In the early morning hours of May 1, 2002, a fire erupted at the Third Coast Industries Friendswood facility, located in an unincorporated area of Brazoria County, Texas. The facility (which blended and packaged motor oils, hydraulic oils, and engine and other lubricants) was inadequately designed and protected to prevent the spread of fire.
Firefighters arrived at the scene within minutes, but had insufficient means to fight the fire, which burned for more than 24 hours. The fire consumed 1.2 million gallons of combustible and flammable liquids and destroyed the site. One hundred nearby residents were evacuated, a local school was closed, and significant environmental cleanup was necessary due to fumes and runoff. No employees or firefighters were injured during the incident..
KEY ISSUES:
• FIRE CONTROL
• CONSENSUS STANDARDS
• FIRE CODES
ROOT CAUSES:
1. Third Coast did not conduct an adequate fire protection analysis to ensure implementation of fire protection measures.
2. The Third Coast facility fire suppression system was inadequate for detecting and warning of fire or smoke or for stopping fire spread.
3. The Third Coast facility lacked adequate control measures to limit the spread of the initial fire.
Image Credit: CSB

Summary
On May 3, 2019, a silicone manufacturing process generated a flammable gas inside an enclosed production building at the AB Specialty Silicones (‘AB Specialty’) facility in Waukegan, Illinois. At approximately
Summary
On May 3, 2019, a silicone manufacturing process generated a flammable gas inside an enclosed production building at the AB Specialty Silicones (‘AB Specialty’) facility in Waukegan, Illinois. At approximately 9:30 p.m., the flammable vapor cloud found an ignition source and ignited, causing an explosion and fire. The flammable vapor originated from the area where AB Specialty was making a silicon hydride emulsion.
The explosion fatally injured four AB Specialty employees and caused serious injury to another AB Specialty employee. At the time of the incident there were nine AB Specialty employees onsite. The explosion heavily damaged the AB Specialty’s production building. Additionally, the force from the explosion was felt up to 20 miles away in the surrounding communities, and some nearby businesses sustained damage from the blast. Post-incident, AB Specialty has resumed some of its operations at another location.
KEY ISSUES:
• FLAMMABLE GAS DETECTION
• FLAMMABLE GAS VENTILATION
Image credit: CSB

Summary
Enbridge responded to an explosion on Line 10 of its Texas Eastern Transmission Co. (Tetco) system in Fleming County, Kentucky, and said Tuesday that it has shut-in a section of
Summary
Enbridge responded to an explosion on Line 10 of its Texas Eastern Transmission Co. (Tetco) system in Fleming County, Kentucky, and said Tuesday that it has shut-in a section of the pipeline and secured the area. No injuries were reported.
The incident has reportedly impacted more than 1 billion cubic feet of daily north-to-south capacity on the system, sending natural gas futures higher after gaining Monday on falling production and higher anticipated demand due to predicted cold weather.
Line 10 is a 30-inch pipeline that is part of Enbridge’s Texas Eastern Natural Gas system.
Toronto-based Enbridge releases a brief statement in response to the blast.
“Enbridge is continuing to respond to the incident that occurred at approximately 5:00 p.m. ET, Monday, May 4, 2020, on its Line 10 natural gas pipeline in Fleming County, Kentucky. There were no injuries,” the company said.
“Our crews are on site and have secured the area. The impacted section of pipe was shut-in following the incident and remains isolated.”
Enbridge said it has notified county, state and federal agencies and officials and reportedly notified customers of a force majeure event resulting in an unplanned outage.
Genscape analyst Josh Garcia said in a note to clients early Tuesday morning that the blast occurred north of its Owingsville Compressor and “just upstream” of where an Enbridge pipeline explosion occurred in 2019.
Image Credit: Lex18
Summary
At about 12:07 a.m. on May 4, 2009, highly flammable vapor, released from a waste recycling process, ignited and violently exploded, severely injuring two employees and slightly injuring two others
Summary
At about 12:07 a.m. on May 4, 2009, highly flammable vapor, released from a waste recycling process, ignited and violently exploded, severely injuring two employees and slightly injuring two others at Veolia ES Technical Solutions, LLC. Multiple explosions afterward significantly damaged every structure on the site. Residences and businesses in the surrounding community also sustained considerable damage. The fire was declared under control by 10:38 a.m. that day.
KEY ISSUES:
• UNSAFE BUILDING SITING
• ATMOSPHERIC RELIEF SYSTEMS
• PLANT EMERGENCY PROCEDURES
ROOT CAUSES:
1. The vent devices were not designed to contain or control hazardous and/or toxic vapor.
2. No record existed of a process hazard analysis (PHA) to evaluate the siting of the lab/operations building so close to the operating units.
Image credit: CSB

Summary
At 3:37 a.m. on May 5, 1988, an explosion occurred in the catalytic cracking unit (CCU) of an oil and gas refinery. The explosion apparently was the result of corrosion
Summary
At 3:37 a.m. on May 5, 1988, an explosion occurred in the catalytic cracking unit (CCU) of an oil and gas refinery. The explosion apparently was the result of corrosion of an 8-inch (200 mm) vapor line. This vapor line, under 270 pounds per square inch (1,900 kPa) pressure, ran from a 10-inch (250 mm) header that originated as the main overhead vapor line from the depropanizer column. The apparent instantaneous line failure released approximately 17,000 pounds (7,700 kg) of hydrocarbon vapor for approximately 30 seconds. A possible ignition source could have been the unit’s superheater furnace. The damage pattern indicated that the explosion was probably an aerial explosion with an epicenter located in the area between the depropanizer and the CCU control room. Employees #1, #2, #4, #5, and #7 were found fatally injured inside the CCU control room as a direct result of the blast. Employee #3 was found fatally injured approximately 30 feet (9.1 m) outside the west side of the CCU control room as a direct result of the blast. Employee #6 was fatally injured while he was exiting the GO-1 South control room. Damage from the explosion radiated one mile (1.6 km) from the center of the explosion and debris could be found as far as five miles (8.0 km) from the center of the explosion. The blast could be heard approximately 25 miles (40 km) away in New Orleans. There were reports that the blast set off burglar alarms in New Orleans. The explosion caused a fire to burn for eight hours at the oil refinery before it was brought under control. Chemicals that escaped during the explosion resulted in cars and homes being covered by a black film. The governor declared a state of emergency in Norco and St. Charles Parish. Seven shell workers were killed during the explosion and 48 residents and Shell workers were injured in the explosion. The explosion released 159 million pounds (72 kt) of toxic chemicals into the air, which led to widespread damage and the evacuating on 4,500 people.
[ Property Damage $288 Million. Estimated Current Value $665 Million ]
Image credit: Fort Myers Fire Academy
Summary
A devastating explosion Tuesday afternoon at an automotive plastics plant in Ottaviano, Italy, killed one worker and injured two, states the Facebook page for the country’s chief firefighting agency. Video posted
Summary
A devastating explosion Tuesday afternoon at an automotive plastics plant in Ottaviano, Italy, killed one worker and injured two, states the Facebook page for the country’s chief firefighting agency.
Video posted by Vigili del Fuoco shows a shattered industrial complex complete with wrecked cars, collapsed fencing and roofs stripped to the structural steel. Likewise, video posted to YouTube by nearby residents shows extensive damage to nearby homes.
Adler Plastics, based in Ottaviano, is a multi-national corporation with 58 plants in 19 countries. The company specializes in plastics used for acoustic and thermal comfort in high value automobiles
Authorities identified the single fatality as Vincenzo Lanza, 55, from Ottaviano. The injured workers were taken to hospitals in Nola and Cardarelli.
What one newspaper described as a ‘crazy roar’ heard more than 10 kilometers away preceded the 4 p.m. blast. That same publication, Il Riformista, said the blast originated in a portion of the facility occupied by ovens used to heat the plastics.
Air quality monitoring of the black smoke rising from the wreckage is in progress, officials said
Image Credit: iNews24.it
Summary
At least 12 people were killed and 129 injured in an explosion and fire at a petrochemicals plant that manufactured polybutadiene. In addition, thousands of people were evacuated from adjacent
Summary
At least 12 people were killed and 129 injured in an explosion and fire at a petrochemicals plant that manufactured polybutadiene. In addition, thousands of people were evacuated from adjacent factories and communities within a three-kilometre-radius of the site. The explosion and subsequent fire sent thick black smoke into the air above the site. The deaths and injuries were as a result of blast injuries, burns, and inhalation of toxic fumes. It was reported that the explosion and fire occurred while workers were cleaning the polymer production line to change between batches, using toluene as a cleaning solvent.
[ Property Damage $143 Million. Estimated Current Value $156 Million ]
Image credit: Rigzone
Summary
Five people have serious injuries after an explosion at Grosvenor coal mine at Moranbah in central Queensland’s Bowen Basin. Key points: – Five workers have suffered serious injuries after an explosion
Summary
Five people have serious injuries after an explosion at Grosvenor coal mine at Moranbah in central Queensland’s Bowen Basin.
Key points:
– Five workers have suffered serious injuries after an explosion at the coal mine
– The injured have significant burns to their torsos and airways
– Mining company Anglo American says the mine has been evacuated and all other personnel are accounted for
The patients suffered burns to their upper bodies and airways and were taken to Moranbah Hospital in a serious condition.
Ambulance crews were called to the scene just after 3:00pm and multiple rescue helicopters were called in.
A spokesperson for Queensland Mines Minister Anthony Lynham said the explosion took place at Grosvenor coal mine, which is operated by Anglo American.
In a statement, mining company Anglo American said it was in the process of evacuating the mine and the emergency response was underway.
“Five people have been injured and transported to hospital. All of the injured people’s families have been contacted,” it read.
Image Credit: ABC News
Summary
A gas leak at an Indian chemical factory has killed at least 11 people and hospitalised hundreds. The styrene tanks had been left unattended due to India’s coronavirus lockdown. The LG
Summary
A gas leak at an Indian chemical factory has killed at least 11 people and hospitalised hundreds. The styrene tanks had been left unattended due to India’s coronavirus lockdown.
The LG Chemical plant, located in Visakhapatnam on India’s east coast, had been offline due to India’s coronavirus lockdown which began on 24 March. Relaxing of lockdown restrictions led to the plant restarting operations, which is when the leak occurred. Maintenance personnel were on-site at the time of the leak.
Two 5,000 t tanks of styrene leaked due a fault in the refrigeration unit, according to The Hindu, which created a styrene vapour cloud that spread around 3 km from the plant and affected five villages. It occurred around 03:00 local time on 7 May and at least 11 people were killed, including two children.
According to The Guardian, the gas caused people to collapse in the streets as they tried to evacuate. Dead cattle were also lying in the streets. Reports suggest 300–1,000 people have been hospitalised, with hospitals already under strain due to the Covid-19 pandemic. Victims suffer from a burning sensation in their eyes as well as breathing difficulties, with some needing ventilators. The BBC reported that according to officials, most should recover.
The gas leak is now under control, according to The New York Times.
The accident echoes the Bhopal tragedy in India in 1984, when a gas leak from a pesticide plant killed thousands and caused chronic illnesses for at least 100,000 people in the area.
Image Credit: AFP
Summary
An explosion, caused by sodium metal reacting with water, occurred in a chemical plant in Mohekou Bengbu City Industrial Park. The fire was put off in 1 h. Source: A web-based
Summary
An explosion, caused by sodium metal reacting with water, occurred in a chemical plant in Mohekou Bengbu City Industrial Park. The fire was put off in 1 h.
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
A 30-inch diameter crude oil pipeline failed and destroyed three spheroids, pumping units, and other equipment. Ignition was caused by motor vehicles.
Summary
A 30-inch diameter crude oil pipeline failed and destroyed three spheroids, pumping units, and other equipment. Ignition was caused by motor vehicles.
Summary
On Tuesday 11 May 2004, at about noon, an explosion occurred at Grovepark Mills, Maryhill, Glasgow which caused the substantial collapse of the former Mill building. As a result, 9
Summary
On Tuesday 11 May 2004, at about noon, an explosion occurred at Grovepark Mills, Maryhill, Glasgow which caused the substantial collapse of the former Mill building. As a result, 9 people lost their lives and 45 people were seriously injured or exposed to the risk of death or injury.
The immediate cause of the explosion was the escape of LPG from the substantially corroded underground pipework at the cracked right-angled bend close to the southern wall of the building, the tracking of the escaped gas into the basement of the building at the west end, the accumulation of the gas in the basement to a point where it constituted an explosive mixture in air, and the ignition of that mixture.
Image Credit: HSE
Topics
11th May 2004
Summary
At least 22 people were injured when a crude oil tanker burst into flames at one of Indonesia\’s busiest ports on Monday (May 11) with rescuers scrambling to reach dozens
Summary
At least 22 people were injured when a crude oil tanker burst into flames at one of Indonesia’s busiest ports on Monday (May 11) with rescuers scrambling to reach dozens trapped on board, an official said.
Two explosions were heard shortly before the blaze erupted on the 250m long Jag Leela, belching huge clouds of thick black smoke into the air.
Firefighters on board another boat battled to put out the inferno on the Indonesia flagged vessel that was docked for repairs at North Sumatra’s Belawan port.
Emergency personnel rushed 22 injured sailors to hospital with dozens more still trapped on the tanker, said local police chief Dayan, who goes by one name.
The cause of the explosion and fire had yet to be determined, he said.
The blaze spread to at least one other vessel docked beside the oil tanker while the force of the explosion caused minor damage to nearby homes, Dayan added.
Image Credit: AFP
Summary
An explosion and fire razed a chemical factory in the Bandar Kinrara Industrial Park Fire & Rescue Department deployed eight fire trucks and 54 fire fighters. It was reported that
Summary
An explosion and fire razed a chemical factory in the Bandar Kinrara Industrial Park Fire & Rescue Department deployed eight fire trucks and 54 fire fighters. It was reported that the spark from the factory’s production floor ignited the highly flammable Hexane
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: The Star
Summary
An electrical discharge in Acton Technologies company caused a fire in a warehouse were acetone was stored. School evacuation Proximate causes: • Hazardous work exposure Source: A web-based collection and analysis
Summary
An electrical discharge in Acton Technologies company caused a fire in a warehouse were acetone was stored. School evacuation
Proximate causes:
• Hazardous work exposure
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Image Credit: Times Leader
Summary
On 15 May, an explosion at a chemicals plant in an industrial zone in Venice, Italy seriously burned two workers and sent clouds of smoke and flames into the sky,
Summary
On 15 May, an explosion at a chemicals plant in an industrial zone in Venice, Italy seriously burned two workers and sent clouds of smoke and flames into the sky, reports Reuters.
Citing local media, Reuters states that the explosion “hit” 3V Sigma, a specialty chemicals company. Reportedly, the blast prompted local authorities to order residents to stay indoors and close windows.
The scene was attended by ambulances and fire services, as well as officials from environmental agency ARPAV.
According to the news agency, an official from the civil protection department, Gianpaolo Bottacin, said that the area was blocked off to prevent the fire from extending beyond the 3V Sigma site. He added that he doubted it would be put out any time soon. The report does not note if or when the fire was extinguished.
Image Credit: Vigili del Fuoco via AP
Summary
A leakage of Carbon disulfide cooling pipe occurred in Ruixing company. 8 killed and 6 injured in the following rescue process. Proximate causes: • Inadequate tools, equipment & vehicles (pipe leaking) Source:
Summary
A leakage of Carbon disulfide cooling pipe occurred in Ruixing company. 8 killed and 6 injured in the following rescue process.
Proximate causes:
• Inadequate tools, equipment & vehicles (pipe leaking)
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
An explosion occurred in a chemical container Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)
Summary
An explosion occurred in a chemical container
Source: A web-based collection and analysis of process safety incidents (https://www.sciencedirect.com/science/article/abs/pii/S0950423016302285)

Summary
A faulty temperature probe on a 600,000-metric-ton-per-year ethylene plant initiated an isolation of the hydrogenation reactor located within the cold section. While the operators were attempting to regain normal control,
Summary
A faulty temperature probe on a 600,000-metric-ton-per-year ethylene plant initiated an isolation of the hydrogenation reactor located within the cold section. While the operators were attempting to regain normal control, the pressure relief system operated. About the same time, fire was noted near grade level at the base of the de-ethanizer column. The source of fuel was believed to have been a flange at the de-ethanizer column reboiler or in the relief system pipe work. Leaking hydrocarbon, mostly propylene at 375 psig, was possibly ignited by hot steam piping. The intense fire rapidly engulfed the adjoining ethylene and propylene distillation columns and spread 180 feet to the storage area. Eventually, one vertical pressurized propane storage tank exploded, its top section traveling 1,500 feet and missing a gas holder by 30 feet. Two other propylene tanks toppled; one onto a pipe rack, and the other against an ethylene tank. All were protected by deluge waterspray systems, which apparently were ineffective under the intense fire exposure. Five of the eight ethylene and propylene tanks collapsed or exploded. The fire also spread to the API separator and to three floating roof tanks. Pipe racks, motor control centers, and pumps were severely damaged or destroyed. A few minutes after the fire brigade responded, the ethylene column released its 9,300 US gallon inventory, destroying one of the plant’s two foam trucks. Assisted by outside fire fighting agencies, the plant fire brigade brought the fire under control over 40 hours and finally extinguished it four days after the initial ignition.
[ Property Damage $74 Million. Estimated Current Value $185 Million ]
Image credit: No credit
Summary
An explosion at Kuraray America on May 19, 2018, injured 21 workers at the EVAL facility in Pasadena, Texas. The facility manufactures ethylene vinyl-alcohol copolymers, sold as EVAL. Kuraray America
Summary
An explosion at Kuraray America on May 19, 2018, injured 21 workers at the EVAL facility in Pasadena, Texas. The facility manufactures ethylene vinyl-alcohol copolymers, sold as EVAL. Kuraray America is a Tokyo-based specialty chemical manufacturer.
During pre-startup pressure-testing activities of a chemical reactor, an abnormal high-pressure condition occurred and over 2,000 pounds of ethylene were released to the atmosphere from a pressure relief valve. The ethylene vapors ignited, resulting in worker injuries. Twenty-one injured workers were transported to off-site medical facilities for treatment.
KEY ISSUES:
• HOT WORK
Image credit: CSB
